N27VX

Substantial
Serious

FAIRCHILD 24-G S/N: 2929

Accident Details

Date
Sunday, August 13, 1995
NTSB Number
MIA95LA203
Location
HAROLD, FL
Event ID
20001207X04328
Coordinates
30.400283, -87.030082
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
2
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

THE ENGINE MISSING FOR UNDETERMINED REASONS, AND THE FAILURE OF THE PILOT IN COMMAND TO MAINTAIN AIRSPEED WHILE TURNING TOWARD A LANDING AREA.

Aircraft Information

Registration
N27VX
Make
FAIRCHILD
Serial Number
2929
Engine Type
None
Year Built
1938
Model / ICAO
24-G FA24
No. of Engines
0

Registered Owner (Historical)

Name
SALE REPORTED
Address
XXX
Status
Deregistered
City
NONE
State / Zip Code
OK 73159
Country
United States

Analysis

On August 13, 1995, about 1110 central daylight time, a Fairchild 24, N27VX, registered to a private owner, crashed shortly after takeoff from McCutchan Strip, Harold, Florida, while on a 14 CFR Part 91 personal flight. Visual meteorological conditions prevailed at the time and no flight plan was filed. The aircraft was substantially damaged and the commercial-rated pilot and one passenger received serious injuries. The flight was originating at the time of the accident.

The pilot stated they suffered a partial loss of engine power while climbing through 75 feet during takeoff. As he made a right turn for an emergency landing on the adjacent highway they suffered "a critical power loss." He made a turn to avoid power lines and does not remember any further details.

The passenger stated the engine "spit" a little while climbing through 250 feet after takeoff. He did not perceive a loss of engine power and power lines ahead of them were not in the way. The pilot made a right turn with about 60 degrees of bank. The aircraft stalled and entered a spin from which they crashed.

Postcrash examination of the engine was performed by an FAA inspector and a mechanic. The engine assembly rotated normally and all cylinders produced compression. The magnetos operated normally. The carburetor bowl contained some clean fuel and no contamination was found. Examination of the carburetor showed the mixture control metering valve assembly locking nut was backed away about three turns and there was no safety wire on the nut. The metering valve assembly was slightly loose in the throttle body. See attached reports.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA95LA203