N1474N

Substantial
None

PIPER J3C-65 S/N: 23140

Accident Details

Date
Sunday, September 10, 1995
NTSB Number
ATL95LA167
Location
MOORESVILLE, NC
Event ID
20001207X04421
Coordinates
35.570968, -80.809700
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The pilot's improper use of the carburetor heat resulting in the formation of carburetor ice and subsequent loss of engine power.

Aircraft Information

Registration
Make
PIPER
Serial Number
23140
Engine Type
Reciprocating
Year Built
1947
Model / ICAO
J3C-65 J3
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
J3C-65

Registered Owner (Current)

Name
TANZER MATTHEW M
Address
5101 KENMONT DR
City
DURHAM
State / Zip Code
NC 27713
Country
United States

Analysis

On September 10, 1995, about 1030 eastern daylight time, a Piper J3C-65, N1474N, collided with trees during a forced landing near Mooresville, North Carolina. The airplane was operated by the pilot/owner under the provisions of 14 CFR Part 91, and visual flight rules. Visual meteorological conditions prevailed. A flight plan was not filed for the personal, local flight. There were no injuries to the private pilot nor his passenger, and the airplane was substantially damaged. Origination of the flight was Bradford Field, a private airstrip, near Huntersville, North Carolina, about 45 minutes prior to the accident.

The pilot reported that they were in cruise flight, about 1400 feet msl (700-800 agl) when the engine lost power. Engine power decreased smoothly, he reported. Carburetor heat was applied for about one minute, then removed, just before an intentional stall into a pine forest, at very slow speed. Immediately prior to the loss of power, the engine was being operated at 2100 rpm. Local temperature and dew point was 76 and 66 degrees F., respectively.(See attached icing probability curves).

The on-scene investigation revealed 1/2 tank of fuel in the main, 5 gallons in the reserve tank, engine oil satisfactory, and throttle linkage intact. The engine examination disclosed heavy soot deposits on the spark plugs, moisture in the carburetor, and the fuel free from containments. The engine operated properly at all power settings during the functional examination. The pilot later stated that he believed carburetor icing had caused the loss of engine power.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ATL95LA167