N135C

Destroyed
Minor

Stinson ST-108-2 S/N: 108-5135

Accident Details

Date
Wednesday, December 27, 1995
NTSB Number
FTW96LA077
Location
LAKE DALLAS, TX
Event ID
20001207X05009
Coordinates
32.880622, -96.649246
Aircraft Damage
Destroyed
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
1
Total Aboard
2

Probable Cause and Findings

the failure of the #6 connecting rod assembly. A factor was the lack of suitable terrain for a forced landing which resulted in a water landing.

Aircraft Information

Registration
N135C
Make
STINSON
Serial Number
108-5135
Engine Type
Reciprocating
Year Built
1947
Model / ICAO
ST-108-2 S108
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
BOWEN BRAD
Address
1010 W AVE E
Status
Deregistered
City
GARLAND
State / Zip Code
TX 75040
Country
United States

Analysis

On December 27, 1995, approximately 0952 central standard time, a Stinson ST-108-2, N135C, registered to, and operated by the student pilot under instruction, as a Title 14 CFR Part 91 instructional flight, was destroyed during a forced landing to water following a loss of power after takeoff from a private airstrip, near Lake Dallas, Texas. Visual meteorological conditions prevailed and no flight plan was filed. The pilot-in-command, a certified flight instructor (CFI), received minor injuries and the student pilot was not injured. After practicing takeoffs and landings, the flight departed the airstrip about 2 minutes prior to the accident, and was en route to Addison Airport, Dallas, Texas.

The CFI reported the following information: After takeoff, while climbing through 500 feet above ground level, the engine "experienced a dramatic and immediate power loss (70-80%) and began surging, all in the low RPM range." The airplane could not sustain level flight. The student pilot was at the controls when the engine started to run rough; however, the CFI assumed control of the airplane during the emergency descent/landing. He attempted to return to the airstrip, however; "although the engine was still running, it was not developing any appreciable thrust." During the descent, he decided to "ditch under control" in a lake to avoid descending into a residential area. Both occupants exited the airplane after the water landing, and swam to shore. The airplane subsequently submerged.

During an engine teardown by the owner, it was discovered that the #6 connecting rod had "failed."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW96LA077