N5079J

Substantial
Serious

Cessna 310R S/N: 310R0199

Accident Details

Date
Wednesday, January 24, 1996
NTSB Number
MIA96LA071
Location
FORT PIERCE, FL
Event ID
20001208X05178
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
3
Uninjured
0
Total Aboard
4

Probable Cause and Findings

failure of the pilot to follow emergency procedure(s) and/or feather the respective propeller after loss of power in the left engine for an undetermined reason. The undetermined loss of power (left engine) was a related factor.

Aircraft Information

Registration
N5079J
Make
CESSNA
Serial Number
310R0199
Engine Type
Reciprocating
Model / ICAO
310R C310
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
CORDAIR INC
Address
C/O M WILLIS & SON BT WORKS
Status
Deregistered
City
MARSHALLBERG
State / Zip Code
NC 28553
Country
United States

Analysis

On January 24, 1996, about 1119 eastern standard time, N5079J, a Cessna 310R crashed in Fort Pierce, Florida, while on a 14 CFR Part 91 personal flight. Visual meteorological conditions prevailed at the time and a VFR flight plan had been filed. The airplane was substantially damaged. The private pilot and three passengers received minor injuries, and one passenger was seriously injured. The flight originated from Freeport, Bahamas, with a stop at North Eleutria Island.

The pilot stated that on left base for landing the left engine failed and he did not feather the propeller. He further stated that the right engine would not produce full power. He attempted to land on a road and struck a tree. There was an extensive postcrash fire.

According to the pilot's statement on the NTSB Form 6120.1/2, when they departed North Eleutria Island, there was "20 gallons in each main [tank], 30 [gallons] in each auxiliary tank, 20 [gallons] in left wing locker...duration of the flight 1+40, fuel consumption 31 gallons per hour," or an approximate burn of 52 gallons of fuel.

The pilot further stated that while at a cruise altitude of 6500 feet, he "switched" to the auxiliary tanks, and had "drained the left wing locker tank" en route to Freeport. Between Freeport and Fort Pierce, he switched back to the main tanks, and was on the mains when he landed.

The pilot told the police that after performing the landing check list he extended the landing gear. He then turned left onto base leg when the "left engine quit." He went to full power on the right engine, but was "unable to get full power." Examination of the wreckage revealed that the left engine propeller was not feathered.

Further examination of the wreckage revealed that the landing gear was down, and the left engine cowling was intact. The left engine and cowling did not display any fire damage. The right engine and right side of the airplane had been consumed by fire damage.

Both fuel selectors were found on the main fuel tanks. The left engine was placed on a test stand and a test run was conducted. No discrepancies were found during the engine test run.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA96LA071