N8951N

Substantial
Minor

PIPER PA-32-300 S/N: 32-40753

Accident Details

Date
Tuesday, February 13, 1996
NTSB Number
ATL96TA047
Location
WINDERMERE, FL
Event ID
20001208X05221
Coordinates
28.489711, -81.529991
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

the use of improper connecting rod bolts, failure of the overhaul facility to record the correct overhaul date on the work orders for the stored connecting rod assemblies, and subsequent failure of the connecting rod bolts.

Aircraft Information

Registration
N8951N
Make
PIPER
Serial Number
32-40753
Engine Type
Reciprocating
Year Built
1970
Model / ICAO
PA-32-300 PA32
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SMITH JAMES E
Address
RT 1
Status
Deregistered
City
MAYFIELD
State / Zip Code
KY 42066
Country
United States

Analysis

On February 13, 1996, about 1304 eastern standard time, a Piper PA-32-300, N8951N, collided with a tree during a forced landing at Windermere, Florida. The aircraft was operated by the Florida Department of Agriculture under the provisions of Title 14 CFR Part 91 and visual flight rules. A flight plan was not filed for the public use flight, and visual meteorological conditions prevailed. The commercial pilot sustained minor injuries; the aircraft was substantially damaged. The aircraft departed Kissimmee Airport, Kissimmee, Florida, at 1100 on the same day.

The pilot stated that while in cruise flight on a forest fire spotting mission, the engine began to run roughly, vibrating the entire aircraft. Oil started spraying from the engine onto the windscreen, then the engine quit. The pilot executed an emergency landing, touching down in an orange grove, and collided with a tree.

An engine examination revealed that bogus connecting rod bolts had been used in the engine. The bolts in two connecting rods failed, resulting in the failure of the engine. Investigation determined that the bolts were manufactured in the 1980s, and became available in the Unites States market on February 15, 1994. The bolts were obtained by the repair station in June, 1994, and installed in connecting rod assemblies that were in storage. The overhaul date on the work order for the stored rod assemblies was not changed at that time, and continued to indicate an overhaul date of February 9, 1994. The stored rod assemblies were then installed in the engine during an overhaul in October 28, 1994. On March 17, 1995, Airworthiness Directive (AD) 95-07-01 was issued to inspect engines with connecting rod bolts installed on or since February 15, 1994. The AD was not complied with on the engine because the repair station certified that the rod assemblies had been overhauled on February 9, 1994, before the effective date of the AD.

The FAA conducted an investigation to locate and remove from the system all defective connecting rod bolts from the original manufacturer.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ATL96TA047