N7713Q

Substantial
Minor

Cessna T310Q S/N: 310Q0213

Accident Details

Date
Wednesday, April 10, 1996
NTSB Number
CHI96LA129
Location
MINNEAPOLIS, MN
Event ID
20001208X05531
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

the inadequate fuel supply for the intended flight which resulted in fuel exhaustion. Factors related to the accident were the pilot operating the airplane with an inoperative fuel gauge and the embankment which the airplane traveled down during the forced landing.

Aircraft Information

Registration
N7713Q
Make
CESSNA
Serial Number
310Q0213
Engine Type
Reciprocating
Model / ICAO
T310Q C310
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
MURPHY MOTORS INC
Address
1801 2ND AVE W
Status
Deregistered
City
WILLISTON
State / Zip Code
ND 58801-3401
Country
United States

Analysis

On April 10, 1996, at 1017 central daylight time, a Cessna T310Q, N7713Q, collided with the terrain during a forced landing on a road in Minneapolis, Minnesota. The forced lading was being made as a result of a loss of engine power on both engines. The airplane was substantially damaged and the private pilot received minor injuries. The flight was operating in visual meteorological conditions on an IFR flight plan. The flight departed Williston, North Dakota, at 0740 cdt.

The pilot stated he departed Williston with the auxiliary fuel tanks full and the main fuel tanks 1 to 2 inches from full fuel. He stated that 50 miles from his destination, Crystal Airport, Minneapolis, Minnesota, the right engine quit followed 10 minutes later by the left engine quitting.

A transcript of the communications between the pilot of N7713Q and the Minneapolis Approach Controller who was working the airplane indicated that at 1007 the pilot stated, "Approach, I'm getting pretty low on fuel, can you direct me to the airport?" The controller responded that he was 16 miles away form the airport. One minute later at 1008, the pilot reported "...I'm losing an engine." At 1011, the pilot reported "...13Q has a dead right engine." The controller responded that the airport was now 8 1/2 miles away. At 1015, the pilot reported "Complete fuel loss, I'm going to have to put her down."

The pilot stated he waited until the last minute to lower the gear in order to clear trees during the forced landing. The airplane touched down on a road without the gear fully extended. It slide off the side of the road and down an slight embankment where it contacted a road sign. The fire/rescue workers who responded to the scene reported that approximately 10 to 15 gallons of fuel spilled from the airplane during the impact sequence. According to the Federal Aviation Administration (FAA) Inspectors who arrived on the scene, the main and auxiliary fuel tanks had ruptured during the impact sequence. The fuel system was inspected and no signs of previous fuel leakage were found.

Additional Information

The pilot reported that the right fuel tank gauge had been inoperative and it indicated a full fuel tank for the entire flight. The pilot stated the airplane had last been refueled on March 12, 1996, and that he had not flow the airplane since. According to an FAA Inspector, maintenance was performed on the airplane in December, 1995. Between that time and the time of the accident the hobbs meter showed the airplane had been flown 3.9 hours. However, the pilot's logbook showed he had flown this airplane a total of 22.4 hours since the December maintenance.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI96LA129