N52MA

Destroyed
Minor

Cessna 152 S/N: 152-83231

Accident Details

Date
Thursday, May 23, 1996
NTSB Number
FTW96LA225
Location
BRIDGEPORT, TX
Event ID
20001208X05773
Coordinates
33.200656, -97.749855
Aircraft Damage
Destroyed
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

the pilot's improper preflight by failing to ensure the mixture control was properly set before takeoff, and his failure to abort the takeoff (while there was sufficient runway remaining).

Aircraft Information

Registration
N52MA
Make
CESSNA
Serial Number
152-83231
Engine Type
Reciprocating
Model / ICAO
152 C152
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
BRIDGEPORT FLIGHT TRAINING CTR INC
Address
RTE 2 BOX 189A
Status
Deregistered
City
BRIDGEPORT
State / Zip Code
TX 76426
Country
United States

Analysis

On May 23, 1996, at 1750 central daylight time, a Cessna 152, N52MA, owned and operated by Bridgeport Flight Training Center, sustained substantial damage during takeoff from the Bridgeport Municipal Airport in Bridgeport, Texas. The student pilot received minor injuries. Visual meteorological conditions prevailed for the Title 14 CFR Part 91 local solo instructional flight. A flight plan was not filed.

The student pilot was practicing short field takeoffs. According to witnesses, the airplane did not sound like it was at full power during the takeoff roll. The witnesses stated that, although the airplane did get airborne, it seemed to "wallow" at about 10 feet AGL all the way down the 4,009 foot runway. The pilot reported that, after he rotated and became airborne, "the aircraft just started to sink and loose airspeed. I tried to keep it up as much [as] I could, but to no response." He further reported that he "continued in this state, proceeding down the runway not aware of my close proximity to the trees." The airplane impacted the trees at the end of the runway.

The FAA inspector reported that the pilot said that, "he had been taxiing with the mixture partially to the lean position and did not remember if he pushed it all the way rich prior to takeoff, and during [the] roll down [the] runway he heard a noise that could have been from a lean mixture setting."

Inspection by the FAA inspector revealed that the right wing was "broken" at the outboard end of the flap with the tip bent back towards the tail, and the area from the cockpit control panel forward separated from the fuselage. The airplane contained fuel, although the exact amount could not be determined due to leakage from broken fuel system components. When the cockpit area was examined, the mixture control was in a leaned position.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW96LA225