N906UP

Unknown
None

Boeing 727-30C S/N: 19314

Accident Details

Date
Friday, June 14, 1996
NTSB Number
CHI96IA200
Location
CHICAGO, IL
Event ID
20001208X05915
Aircraft Damage
Unknown
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

low pressure in the fuel lines caused when the crossfeed valve was closed and the boost pumps to the effected fuel tank were turned off, a fuel pressure surge (spike) accompanied by a rapid drop in high pressure pump output and burner line pressures, when boosted fuel was reintroduced to the system, which resulted in temporary fuel starvation to the three engines, and the inadequate aircraft/equipment design by production personnel (STC holder). A factor which contributed to this incident was the flight engineer's management of the fuel system.

Aircraft Information

Registration
N906UP
Make
BOEING
Serial Number
19314
Engine Type
Turbo-jet
Year Built
1967
Model / ICAO
727-30C B721
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
3

Registered Owner (Historical)

Name
UNITED PARCEL SERVICE CO
Address
1400 N HURSTBOURNE PKWY
Status
Deregistered
City
LOUISVILLE
State / Zip Code
KY 40223
Country
United States

Analysis

HISTORY OF FLIGHT

On June 14, 1996, at 0118 central daylight time (cdt), a Boeing 727-30C, N906UP, operated as United Parcel Service (UPS) flight 9601, experienced a total loss of power on all three engines, and a subsequent loss of electrical generating power, during an en route descent in preparation for landing at Greater Rockford Airport, Rockford, Illinois. The crew declared an emergency and diverted to Chicago, Illinois. A landing was made at Chicago O'Hare International Airport with all engines operating and electrical generating power restored. Night visual meteorological conditions prevailed at the time of the incident. The positioning flight was being conducted under 14 CFR Part 91. An IFR flight plan was on file. No injuries were reported by the three flight crew members, and no damage to the airplane occurred. The flight originated at Louisville, Kentucky, at 0017 cdt.

The flight crew stated that the airplane lost engine power after beginning a descent from 22,000 feet mean sea level (MSL). The power was not restored to the engines until the airplane was on the approach to runway 32R (10,000' x 150') at the O'Hare airport, and approximately 1,000 feet above the ground. Emergency electrical power was available to the crew throughout the descent. The crew reported normal indications throughout the flight until beginning the descent for landing. The flight engineer said that prior to the descent, he had configured the fuel system to crossfeed between the fuel tanks, so as to reduce a slightly higher fuel quantity indication in the right wing tank, and level the fuel amounts in all three tanks. The crew stated that the fuel boost pumps in the center tank were turned off before the crossfeed valve was opened for the number two engine fuel lines. The crew indicated that the crossfeed valves to the other two fuel manifolds may have been activated shortly after. The first indication of a malfunction was the simultaneous failure of all three of the generators.

A Systems Group was formed on June 14, 1996. The group conducted an examination of the airplane at the UPS base at Chicago O'Hare Airport. The group concluded their field examination on June 27, 1996. A copy of the Systems Group Chairman's Report is attached as an addendum to this report.

AIRCRAFT INFORMATION

The airplane was a Boeing 727-30C, N906UP, serial number 19314, owned and operated by United Parcel Service. The airplane had been modified under Supplemental Type Certificate (STC) Number SA8472SW, issued on November 25, 1992, for installation of three Rolls Royce Model TAY 651-54 engines, and Dee Howard Company TR6510 thrust reversers, by Dee Howard Company of San Antonio, Texas. A copy of the STC Number SA8472SW, the type certificate data sheet, and the Federal Aviation Administration (FAA) STC issue paper are attached as addendums to this report.

The airplane was referred to by UPS as a Boeing 727-100QF.

FLIGHT RECORDERS

The Digital Flight Data Recorder (DFDR), was removed from the incident airplane and sent to the NTSB's Vehicle Performance Laboratory for readout and evaluation. A successful DFDR readout was performed. The report of that readout is attached as an addendum to this report.

The DFDR data indicated that prior to the recorded power loss, N906UP was at 20,000 feet MSL, in a slight descent, heading 315 degrees, and with N1 values on all three engines steady at 36 percent. This was the last recorded data before the power loss occurred on the DFDR. The next recorded event of the DFDR was with the aircraft at 1,600 feet MSL, pitch 3 to 5 degrees nose up, and all engines showing an N1 of near zero (0) percent. Approximately 45 seconds after the recorder power was restored, the number 2 and 3 engines rapidly spooled up (over an elapsed time of 5 seconds) to an N1 of 93 percent. The number 1 engine followed 20 seconds later. The DFDR recorded a landing at the O'Hare Airport approximately 50 seconds later.

The recorded data received from the DFDR was verified for accuracy by examining previous performance of the airplane also recorded on the medium. This was done in order to determine if the data received by the recorder was consistent with takeoff, cruise, and normal landing characteristics of the aircraft. The data was found to be consistent with the normal operation of the aircraft.

There was no usable data on the Cockpit Voice Recorder (CVR).

TESTS AND RESEARCH

Subsequent to the incident, the airplane was subjected to a detailed inspection. There was no apparent damage to the airplane, its systems, or associated controls. At the inception of the investigation, the engine controls and switches were found in the normal shutdown positions. The aircraft pneumatic systems were examined for failures or malfunctions. During ground tests, the pneumatic systems functioned normally. The engine instruments were examined for failures or malfunctions. The instruments operated normally during the ground tests. Examination of the engine controls did not reveal any miss- rigging, malfunctions, or failures. The flight instrumentation system showed no apparent damage. The flight controls were examined for rigging, deflection, and malfunctions. They operated normally during ground tests with no malfunctions noted.

The electrical system's examination revealed no apparent damage. During ground tests, the three engine driven generators and the Auxiliary Power Unit operated normally. Examination of the circuit breaker panels revealed no evidence of malfunction. The hydraulic system was examined for evidence of malfunction or failure; none was found. The powerplants were examined for evidence of fire, failures, leaks, or other malfunctions. No evidence was found that would indicate any malfunctions.

The airplane had been converted by a Supplemental Type Certificate (STC) to remove the original powerplants and install Rolls Royce Tay 651-54 engines and Rolls-Royce supplied engine accessories. The original fuel tanks, lines, valves, manifolds, boost pumps, and filters remained.

The airplane fuel system consists of three tanks; a left, right, and center fuel tank. In normal operations each tank feeds a respective engine; i.e., right tank to right engine, etc. Each tank contains multiple fuel boost pumps, a single fueling port for all tanks, a fuel dump valve, a crossfeed valve, associated lines, check valves, and quantity indicating system components. There are two fuel shutoff valves for each powerplant in the fuel system; one airframe mounted engine shutoff valve, and one high pressure fuel shutoff valve on its associated engine.

The fuel system crossfeed valves and plumbing allow fuel to be selected from any tank to feed any of the three powerplants through a crossfeed manifold. Fuel cannot be transferred from tank to tank. According to the holder of the STC, modifications did not alter any of the original fuel system components.

The fuel tanks were inspected for blockage, debris, and other abnormalities. The individual fuel lines, fuel boost pumps, fuel manifold valves, and check valves were pressure tested, inspected, then operationally tested, with no anomalies found. Each of the individual boost pumps were isolated from their respective systems and tested with normal indications.

Ten uninstrumented flight tests were conducted on the incident airplane and two other UPS B-727 airplanes with the Rolls Royce Tay 651-54 engine conversion, between June 28, 1996 and July 10, 1996. Parameters for the flight tests were established so as to protect one engine from flameout when attempting to duplicate the scenario as best recalled by the flight crew on the morning of June 14, 1996. In all but the first flight, the crews were able to duplicate multiple engine flameouts at different altitudes, and with the airplane's fuel system set in various configurations. In the first flight, the airplane was not configured properly to duplicate the engine flameout scenario. An eleventh uninstrumented flight test was conducted on July 14, 1996, with a UPS B-727, which had not undergone the Rolls-Royce Tay 651-54 engine conversion. Using the same test parameters established for the previous 10 flight tests, the flight crew was unable to produce any flameouts in the three Pratt and Whitney JT8D-7 engines.

The flight tests reproduced the scenario of what occurred en route to Chicago, Illinois, on June 14, 1996. First, the number one engine was protected by closing the number one crossfeed valve and keeping the number one engine at cruise power. Next, the number two engine boost pumps were turned off, and the number two crossfeed valves were closed. The number three boost pumps were confirmed "on" and the number three crossfeed valve was opened. Power on the number two engine was reduced to idle and allowed to stabilize for 3 to 5 minutes. Next, the number three engine's power was retarded to idle. The number two crossfeed valve was then opened. The result was consistently the near simultaneous flameouts of number two and three engines. This test sequence usually produced the same results at varying altitudes between 8,000 and 39,000 feet MSL.

On August 1, 1996, it was determined by the FAA, the Dee Howard Company, UPS, and Rolls Royce, that a series of tests, to include on-ground engine and fuel system rig tests, and instrumented flight tests, would be conducted to determine the cause of the engine flameouts, and to develop a hardware modification to the airplane's fuel system/engines, to prevent multiple engine flameouts in various fuel system configurations.

Between August 1, 1996, and May 7, 1997, numerous rig tests and instrumented flight tests were conducted to determine the cause of the multiple engine flameouts. The results of these tests consistently revealed that when the B-727 fuel system is configured with one engine operating in suction feed, air and vapor evolve from the ...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI96IA200