N102KB

Destroyed
None

Beech 23-A24R S/N: MC-45

Accident Details

Date
Friday, June 7, 1996
NTSB Number
LAX96LA221
Location
MODESTO, CA
Event ID
20001208X06026
Coordinates
37.669666, -121.009231
Aircraft Damage
Destroyed
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

fuel exhaustion due to the pilot's inadequate preflight inspection of the aircraft.

Aircraft Information

Registration
N102KB
Make
BEECH
Serial Number
MC-45
Engine Type
Reciprocating
Model / ICAO
23-A24R BE23
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
BARINKA STEPHEN J JR
Address
PO BOX 4334
Status
Deregistered
City
STATELINE
State / Zip Code
NV 89449
Country
United States

Analysis

On June 6, 1996, at 2030 hours Pacific daylight time, a Beech 23-A24R, N102KB, collided with terrain while making a forced landing from closed traffic at the Modesto City-County Harry Sham Field, Modesto, California. The aircraft was destroyed; however; the pilot, who was the sole occupant, was not injured. The aircraft was being operated as a personal flight by the pilot/owner when the accident occurred. The flight originated from Modesto at 1930. Visual meteorological conditions prevailed and no flight plan had been filed.

The pilot reported that during his prior takeoff roll he had experienced what he thought might be an engine problem. He aborted that takeoff, taxied back to the ramp, and performed another complete engine run-up. The engine ran smoothly so he taxied back for takeoff. After takeoff, the pilot reported that he had climbed about 350 feet agl when the engine suddenly quit. Because of his position over the ground, the pilot indicated that he was not in a location from which he could make a safe landing. He attempted to turn toward more favorable terrain. Unable to reach a suitable forced landing area, he was forced to touch down in area with obstructions. The aircraft came to rest about 0.25 miles from the departure end of runway 28L. The pilot told Federal Aviation Administration (FAA) inspectors that he had taken off with half full fuel tanks and with the fuel boost pump switch in the on position.

The FAA airworthiness inspector requested that an airframe and powerplant (A&P) mechanic with inspection authorization (IA) examine the accident aircraft and provide him with a report. The mechanic reported that he checked the fuel in the aircraft and found approximately 3 ounces at the left tank drain valve and approximately .5 gallon at the right tank drain valve. He also found about two drops of fuel in the fuel injection servo, but no fuel at the firewall line fitting. The fuel selector was in the off position. He said that it is a common practice for fire department personnel to turn the fuel selector off after an aircraft is involved in an accident. He did not observe any evidence of fluid leaks or discontinuity in the fuel system.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX96LA221