N3122C

Substantial
None

Cessna 180 S/N: 30921

Accident Details

Date
Monday, July 22, 1996
NTSB Number
ATL96LA112
Location
MEMPHIS, TN
Event ID
20001208X06160
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

Inadequate annual inspection that resulted in the in-flight loss of the fuel system strainer and subsequent fuel starvation. A factor was the lack of suitable terrain for a forced landing.

Aircraft Information

Registration
N3122C
Make
CESSNA
Serial Number
30921
Engine Type
Reciprocating
Year Built
1954
Model / ICAO
180 C180
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
JOHNSON STEVE L
Address
211 S 3RD ST
Status
Deregistered
City
ROBERTSVILLE
State / Zip Code
MO 63072-1422
Country
United States

Analysis

On July 22, 1996, at 1810 central daylight time a Cessna 180, N3122C, collided with a parked automobile and a fence, and was substantially damaged following a forced landing near Memphis International Airport, Memphis, Tennessee. The airline transport pilot was not injured. The personal flight was being conducted under the provisions of Title 14 CFR Part 91 by the pilot. Visual meteorological conditions existed at the time of the accident, and a flight plan was not filed for the cross country flight. The flight departed Griffin-Spalding County Airport, Griffin, Georgia at 1630 eastern daylight time.

According to the FAA inspector, the pilot was cleared to land on runway 27 at Memphis International Airport. About 1 1/2 miles to the east of the airport the pilot reported a loss of engine power. The pilot made a forced landing in a parking lot and collided with an automobile and a fence before coming to rest. The airplane received damage to the wings, fuselage, and right horizontal stabilizer. An inspection by the FAA inspector revealed that the gascolator was missing, and the required safetywire for the gascolator was not found. The last inspection of the engine was done during the annual inspection in July of 1995. The aircraft had been flown 86 hours since the annual inspection.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ATL96LA112