N2506C

Substantial
None

Cessna 170B S/N: 26150

Accident Details

Date
Saturday, December 14, 1996
NTSB Number
CHI97LA043
Location
SAVOY, IL
Event ID
20001208X07144
Coordinates
40.059074, -88.249435
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

the student pilot's failure to maintain directional control. Factors relating to this accident were the student pilot's failure to request another runway and the crosswind.

Aircraft Information

Registration
N2506C
Make
CESSNA
Serial Number
26150
Engine Type
Reciprocating
Model / ICAO
170B C170
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
HERSHMAN WAYNE
Address
PO BOX 112
Status
Deregistered
City
FORTVILLE
State / Zip Code
IN 46040-0112
Country
United States

Analysis

On December 14, 1996, at 1133 central standard time (cst), a Cessna 170B, N2506C, operated by a solo student pilot, sustained substantial damage when on landing roll, the airplane departed the runway and subsequently nosed over. Visual meteorological conditions prevailed at the time of the accident. The personal flight was being conducted under 14 CFR Part 91. No flight plan was on file. The student pilot reported no injuries. The cross-country flight originated at Mount Comfort, Indiana.

In his written statement, the student pilot said the ATIS information at Willard Airport, Savoy, Illinois, called the wind 130 degrees magnetic at 15 knots. On initial contact with the Willard Airport Air Traffic Control Tower, the student pilot informed the tower controller that he was a student pilot and that he was inbound for a full stop landing. The tower controller cleared the student pilot to land on runway 04. On final approach, the student pilot said that he had to use "the wing low with opposite rudder method to a greater degree than I ever used before." On touchdown "the right wing rose to an unacceptable angle. I attempted to lower the wing and stay on the runway, but I lost control of the aircraft." The airplane departed the left side of the runway, "the tires sank causing the aircraft to pitch forward, stopping the engine. The aircraft stood vertical, stopping momentarily, then the wind seemed to blow the airplane over."

The Federal Aviation Administration (FAA) inspector who examined the wreckage at the scene found the left wing rear spar bent downward. The inboard bottom surface of the left wing was bent back and buckled outward near the left fuel tank. The bottom wing skin was opened up along the lateral rivet line. The left wing strut was kinked downward in the middle. The right wing was bent aft and downward. The right rear spar was bent slightly downward. There were skin wrinkles in the bottom inboard surface of the right wing near the right fuel tank. The upper forward cabin frame was bent slightly around the cabin door. The vertical stabilizer was crushed downward and buckled outward. The top portion of the rudder was bent over to the left. The rudder counter weight was located on the right side of the vertical stabilizer. Both propeller blades were bent slightly forward. The spinner was crushed to one side. Flight control continuity was confirmed. No anomalies were found with the engine, engine controls, brakes or other airplane systems.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI97LA043