N2921

Substantial
None

Hoster/Volmer VJ22 (SPORTSMAN) S/N: 206

Accident Details

Date
Friday, December 6, 1996
NTSB Number
MIA97LA035
Location
SEMINOLE, FL
Event ID
20001208X07210
Coordinates
27.839719, -82.780326
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

inadequate maintenance/inspection of the airplane by the pilot/owner, and fuel contamination that resulted in fuel starvation.

Aircraft Information

Registration
Make
HOSTER/VOLMER
Serial Number
206
Engine Type
Reciprocating
Model / ICAO
VJ22 (SPORTSMAN) VJ22
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
SPORTSMAN

Registered Owner (Current)

Name
CARTER BRADFORD J
Address
139 RANKIN ST
City
ROCKLAND
State / Zip Code
ME 04841-2366
Country
United States

Analysis

On December 6, 1996, about 1100 eastern standard time, a Volmer VJ22 amphibious homebuilt airplane, N2921, registered to a private individual, crashed into a canal near Seminole, Florida. Visual meteorological conditions prevailed at the time and no flight plan was filed for the 14 CFR Part 91 personal flight. The airplane was substantially damaged and the private-rated pilot, the sole occupant, was not injured. The flight originated about 30 minutes earlier from Lake Seminole, Seminole, Florida.

The pilot stated that after takeoff from the lake he circled it four times and during a turn while adjusting the fuel/air ratio, the engine experienced a loss of power. He pushed the mixture control full rich, turned on the auxiliary fuel pump, applied full throttle and carburetor heat, but engine power was not restored. He initiated a descent for a forced landing on the lake but unable to clear a bridge ahead, he maneuvered the airplane for a forced landing on a canal. While descending, the right sponson collided with a tree. The airplane then descended into a canal and came to rest upright.

The airplane was recovered and post crash, the engine was started and operated normally. Further examination of the airplane by the pilot/owner revealed blockage of the fuel tank outlet screen. The pilot/owner also stated that he had noticed in the past similar material in the gascolator screen. He further stated that the fuel tank had been out of the airplane 20 years and had been reinstalled in May of 1996. Fuel quantity was reportedly sufficient to sustain engine operation.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA97LA035