N52958

Substantial
Serious

Charles J. Keuthan ZEPHYR II S/N: Z2AK018

Accident Details

Date
Monday, March 31, 1997
NTSB Number
MIA97LA112
Location
BUNNELL, FL
Event ID
20001208X07607
Coordinates
29.460636, -81.250251
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

Inadvertent stall/mush by the pilot while maneuvering for a forced landing. Contributing to the accident was the partial loss of engine power due to a partial failure of the top compression ring of one of the cylinders.

Aircraft Information

Registration
N52958
Make
CHARLES J. KEUTHAN
Serial Number
Z2AK018
Engine Type
Reciprocating
Year Built
1995
Model / ICAO
ZEPHYR II BPAT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
KEUTHAN CHARLES
Address
6896 BABCOCK ST SE
Status
Deregistered
City
PALM BAY
State / Zip Code
FL 32909
Country
United States

Analysis

On March 31, 1997, about 1745 eastern standard time, a homebuilt Zephyr II, N52958, registered to a private individual, collided with terrain following an in-flight loss of control during a forced landing after takeoff from the Flagler County Airport, Bunnell, Florida. Visual meteorological conditions prevailed at the time and no flight plan was filed for the 14 CFR Part 91 personal flight. The airplane was substantially damaged and the private-rated pilot, the sole occupant, sustained serious injuries. The flight originated about 5 minutes earlier from the Flagler County Airport.

The pilot stated that during the upwind leg after takeoff about 300 feet above ground level (agl), the engine experienced an rpm drop from 6,200 to between 2,500 and 3,000. He then initiated a turn downwind and then again turned upwind and when the flight was about 75 feet agl, he encountered loss of elevator control. The airplane then descended nose low and impacted the ground adjacent to the intended touchdown location.

Postcrash examination of the engine revealed a 1/4 inch section of the top compression ring was missing with an associated scar on the piston. Fuel contamination was not noted and there was no evidence of detonation or blockage of the air filter. Both the choke levers were determined to be closed.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA97LA112