N52507

Substantial
None

Boeing Stearman B75N1 S/N: 75-2743

Accident Details

Date
Sunday, April 6, 1997
NTSB Number
MIA97LA115
Location
COLUMBIA, SC
Event ID
20001208X07772
Coordinates
33.940689, -81.150733
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The pilot's inadequate planning/decision and failure to assure an adequate supply of fuel was on board the airplane.

Aircraft Information

Registration
N52507
Make
BOEING STEARMAN
Serial Number
75-2743
Engine Type
Turbo-jet
Year Built
2000
Model / ICAO
B75N1 B752
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
THOMPSON AIRE INC
Address
13825 AVALON RD
Status
Deregistered
City
WINTER GARDEN
State / Zip Code
FL 34787
Country
United States

Analysis

On April 6, 1997, at about 1107 eastern daylight time, a Boeing B75N1, N52507, registered to Training Services Inc., operating as a 14 CFR Part 91 personal flight, experienced a total loss of engine power on descent for landing at Columbia, South Carolina. The pilot made a forced landing to a road about 1 1/2 miles northeast of the airport, colliding with power lines. Visual meteorological conditions prevailed and no flight plan was filed. The airplane sustained substantial damage. The private pilot and one passenger reported no injuries. The flight originated from Roxboro, North Carolina, about 2 hours 37 minutes before the accident.

The pilot stated he started a descent in preparation for landing when the engine quit without any power reduction. He made a left turn looking for a forced landing area, and made a distress call. The engine started by itself and quit again about 15 to 20 seconds after it started. He elected to make a forced landing to a highway. The airplane collided with power lines on final and came to a complete stop on the road.

The pilot stated in an interview with an FAA Airworthiness inspector after the accident, that he was a practical man and he thought he exhausted his fuel supply.

Examination of the airplane revealed the fuel tank was not ruptured. No fuel was present in the fuel tank. A small of fuel (about two ounces) was drained from the left and right fuel drains. The fuel bowl contained about one ounce of fuel and the fuel strainer was clean. There was no evidence of leakage or defects with the fuel system.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA97LA115