N2362K

Substantial
Minor

Piper PA-38 S/N: PA-38-112

Accident Details

Date
Tuesday, May 27, 1997
NTSB Number
SEA97LA123
Location
FRUITLAND, UT
Event ID
20001208X08035
Coordinates
40.149066, -110.820785
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The pilot's failure to maintain clearance from mountainous terrain. Factors include his improper inflight decision to attempt to fly through a mountain pass under high density altitude conditions in an aircraft that was operating near the limits of its performance capability, high density altitude, downdrafts, and mountainous terrain.

Aircraft Information

Registration
N2362K
Make
PIPER
Serial Number
PA-38-112
Engine Type
Reciprocating
Year Built
1979
Model / ICAO
PA-38 PA38
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
STEVENS THOMAS V
Address
341 CHURCH ST
Status
Deregistered
City
LAYTON
State / Zip Code
UT 84041-3107
Country
United States

Analysis

On May 27, 1997, approximately 1700 mountain daylight time, a Piper PA-38, N2362K, impacted the terrain while maneuvering in steep mountainous terrain about 10 miles south of Fruitland, Utah. The private pilot and his passenger, who held a commercial pilot certificate, received minor injuries, and the aircraft, which was being operated by U.S. Aviation of Ogden, Utah, sustained substantial damage. The 14 CFR Part 91 personal pleasure flight, which had departed Duchesne, Utah about 10 minutes earlier, was en route to Ogden, Utah at the time of the crash. No flight plan had been filed, and the flight was being conducted in visual meteorological conditions.

Earlier in the day, the pilot had flown from Ogden, Utah to Duchesne, Utah, and was on the return flight when the accident occurred. According to the pilot, he was trying to fly through a pass that was more than 8,500 feet high. He said that the aircraft had been operating normally, but that he encountered wind conditions which created downdrafts, and the aircraft started to sink toward the terrain. The pilot attempted to get the aircraft to climb, but it descended into the terrain, impacting the ground approximately 8,300 feet above sea level (MSL).

Post-accident performance calculations determined that the density altitude at the time of the accident was greater than 10,000 feet, and according to the PA-38 Pilot's Operating Handbook, the aircraft's climb rate would be less than 100 feet per minutes under those conditions.

The pilot, who was a French national who had come to the United Stated in order to receive flight training, returned to France without completing an NTSB Form 6120.1/2.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA97LA123