Summary
On July 20, 1997, a Goode AVID FLYER MK-IV (N4356H) was involved in an incident near Nikiski, AK. All 2 people aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: The pilot's inadequate compensation for wind conditions. Factors were the sudden windshift, and the pilot's lack of seaplane certification.
On July 20, 1997, at 1130 Alaska daylight time, an Avid Flyer float equipped airplane, N4356H, impacted the water during takeoff from Parsons Lake, Alaska, 10 miles northeast of Nikiski, Alaska. The airplane sustained substantial damage. The private certificated pilot and single passenger were uninjured. The experimental airplane was manufactured and operated by Audie D. Goode of Nikiski, Alaska. The flight was conducted under 14 CFR Part 91 as a personal flight, and visual meteorological conditions prevailed at the time of the accident.
The pilot stated that after takeoff, the wind shifted from a headwind to a gusting crosswind, and the airplane could not maintain a climb.
This incident is documented in NTSB report ANC97LA108. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N4356H.
Accident Details
Probable Cause and Findings
The pilot's inadequate compensation for wind conditions. Factors were the sudden windshift, and the pilot's lack of seaplane certification.
Aircraft Information
Registered Owner (Historical)
Analysis
On July 20, 1997, at 1130 Alaska daylight time, an Avid Flyer float equipped airplane, N4356H, impacted the water during takeoff from Parsons Lake, Alaska, 10 miles northeast of Nikiski, Alaska. The airplane sustained substantial damage. The private certificated pilot and single passenger were uninjured. The experimental airplane was manufactured and operated by Audie D. Goode of Nikiski, Alaska. The flight was conducted under 14 CFR Part 91 as a personal flight, and visual meteorological conditions prevailed at the time of the accident.
The pilot stated that after takeoff, the wind shifted from a headwind to a gusting crosswind, and the airplane could not maintain a climb. He stated that he intentionally landed back onto the water when it became apparent he would not clear trees which were located on the shoreline. The airplane landed hard, and both floats separated from the airplane. The cabin doors were unable to be opened, and both occupants exited through the broken Lexan roof.
The pilot did not have a seaplane rating.
The Alaska State Trooper who responded to the accident site stated that the winds were observed changing direction as he walked around the lake.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ANC97LA108