N3359P

Destroyed
Fatal

Beech B-60 S/N: P400

Accident Details

Date
Sunday, July 20, 1997
NTSB Number
CHI97FA220
Location
SPRINGFIELD, MO
Event ID
20001208X08310
Coordinates
37.210338, -93.350173
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
4
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
4

Probable Cause and Findings

The pilot's fuel mismanagement and his failure to maintain adequate airspeed which resulted in fuel exhaustion followed by the loss of power in one engine and the loss of aircraft control. Contributing was the pilot's failure to refuel the aircraft, the pilot's failure to feather the propeller of the non-operating engine, and his extension of the landing gear.

Aircraft Information

Registration
N3359P
Make
BEECH
Serial Number
P400
Engine Type
Reciprocating
Model / ICAO
B-60 BE60
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
CORPORATE AIRCRAFT MANAGEMENT INC
Address
201 S WALNUT ST
Status
Deregistered
City
ASHLAND
State / Zip Code
MO 65010-9432
Country
United States

Analysis

History of Flight

On July 20, 1997, at 1630 central daylight time (All times CDT), a Beech B-60, N3359P, was destroyed when it impacted terrain two miles northeast of the Springfield/Branson Regional Airport, Springfield, Missouri. The pilot reported that he was having engine problems and he attempted to return to the airport. The airline transport pilot, a pilot rated passenger, and two passengers received fatal injuries. The 14 CFR Part 91 flight departed the Springfield/Branson Regional Airport en route to the Spirit of St. Louis Airport, Chesterfield, Missouri. Visual meteorological conditions prevailed and a VFR flight plan had been filed.

The airplane had departed the Spirit of St. Louis Airport about 0930 and landed at the Springfield/Branson Regional Airport about 1020. The pilot did not request aircraft servicing or fuel. Later that day the pilot and passengers returned and prepared for departure.

An aircraft service lineman at the Springfield/Branson Airport reported that the pilot in the left seat "could have been heavy set" and was wearing a dark tee shirt. The autopsy indicated that the pilot was wearing a knit navy blue and green shirt and weighed over 250 pounds.

At 1610, the pilot called the ground controller and obtained taxi instructions for a VFR flight back to the Spirit of St. Louis Airport. The pilot received taxi instructions for a runway 22 takeoff.

At 1615, the airplane departed and turned on course to the Spirit of St. Louis Airport.

Radar data indicated that the airplane departed to the northeast after takeoff. The first radar "hit" was at 1619:58 and the airplane was about 3.5 nm to the southeast of the field at 2,800 feet mean sea level (msl) and climbing at a rate of 750 fpm.

At 1621, the airplane was about 5 nm east of the airport at 4,300 feet msl. The airplane was about 3,033 feet above ground level (agl).

Witnesses reported that they heard a twin engine airplane with engine problems at about 1615. The location of the witnesses when they observed the airplane was about three miles east of the Springfield Regional Airport. The witnesses reported hearing the airplane's engine/s sputtering, cutting out, or backfiring. They reported seeing the airplane flying, wings level, to the northeast.

At 1621:34, the radar data indicated that the airplane had started a descent on a northeasterly heading. The average rate of descent was about 402 fpm.

At 1624:59, the airplane's altitude was 2,800 feet msl and about 12 nm to the northeast of the airport, about 7 nm further to the northeast from the initial descent point.

At 1624:59, the airplane started a left hand descending turn. The radar data indicated that the airplane made a 180 degree turn and was heading to the southwest.

At 1626.35, the last radar hit on the airplane indicated that it was at 2,200 feet msl and about 10 miles to the northeast of the airport. The airplane was about 933 feet agl.

At 1626:38, the pilot contacted the Springfield local air traffic controller. At 2126:41 the pilot reported, "Yes, sir, we need to return to the airport."

At 2126:54, the controller directed the pilot to fly a 210 degree heading and informed the pilot that he would sequence the airplane in for landing behind a Beech 1900 that was fifteen miles out from the airport.

At 2127:13, the pilot responded, "Okay, ah, we may, ah, not be able to do that. We're going to let you know here in just a minute."

At 2127:18, the controller asked, "Are you experiencing any difficulties?" The pilot responded, "Yes, sir."

At 2127:21, the controller asked, "Can you give me any, ah, information right now?"

At 2127:23, the pilot responded, "Ah, negative. Stand by a minute."

At 2148:49, the pilot informed the controller that, "...ah, we've got a partial engine failure on the left side. We're going to have to limp it on in."

At 2128:54, the controller told the pilot, "Okay, go straight in to runway two zero, sir." The pilot acknowledged landing runway 20.

At 2129:22, the controller asked, "Duke, ah five niner poppa, you want the equipment?"

At 2129:25, the pilot responded, "Ah, not at this point. We're gonna see if we can't make the airport here."

At 2129:36, the controller cleared the airplane to land on runway 22.

At 2129:39, the pilot responded, "Okay, we don't have the airport."

At 2129:41, the controller asked, "Okay, what's your heading?"

At 2129.42, the pilot said, "Isn't going to work. We're gonna have to put it down."

At 2129:44, the controller asked, "Your landing at your present position?"

At 2129:46, the pilot responded, "Ah yeah. We're looking for a field down here."

At 2129:49, the controller responded, "All right, sir. Thank you very much."

There were no further communications from the pilot.

Witnesses reported seeing a twin engine airplane flying to the southwest at a low altitude at about 1630. The location of the witnesses was about .5 to 1.5 miles to the northeast of the accident site. The witnesses reported that they did not hear any backfiring or sputtering noises from the airplane's engines. They reported that both propellers were turning.

A witness reported that he saw the airplane flying through a valley about 1/8 mile to the east of his farmstead. He reported that the airplane was flying north to south "straight down the road." He reported that the airplane was flying 50 to 100 feet below the tree line but above the telephone poles. He reported that the airplane was level, the props were turning, the flaps and gear were up, and the noise sounded like full power. He reported that the engines were not sputtering. He reported that the airplane climbed 50 to 100 feet in order to clear the trees at the south end of the valley where the terrain was higher. The airplane went out of his field of view.

He reported that his wife saw the airplane momentarily. He reported that she saw the airplane get over the trees. She did not see any abrupt maneuvers.

A third witness reported he saw the airplane climb over the trees. He reported that the airplane missed the powerlines but was, "struggling to get over the powerlines." He reported that everything went up in flames. He reported that a little wind was blowing to the northeast. He reported that the local firefighters put out the grass fire, and that the airport firefighters put out the aircraft fire.

Personnel Information

The pilot was an airline transport rated pilot with single and multi-engine land ratings. He held a First Class medical certificate. He had a total of about 10,734 hours of flight time. 7,643 hours were in multi-engine aircraft. In the last 12 months he had logged 46 hours in the accident aircraft. The aircraft operator reported that the pilot initially began flying a B-60 in 1980, but logbooks covering that time period were not obtained.

The pilot was an employed pilot of the aircraft operator. The operator reported that the pilot was meticulous and conscientious in his approach to flying. He reported that the pilot had checked-out the four company pilots in the B-60.

The pilot rated passenger in the right seat of the airplane was an airline transport rated pilot with single and multi-engine land ratings. He held a First Class medical certificate. He had over 20,500 total flight hours.

The operator reported that the pilot rated passenger was a friend of the pilot. He reported that the pilot and pilot rated passenger were planning a fishing trip to Canada for the following week. He reported that the purpose of the flight to Springfield, Missouri, was a pleasure flight in order to purchase fishing equipment. The operator reported that the flight to Springfield was not an instructional flight or an indoctrination flight.

Aircraft Information

The airplane was a twin engine Beech B-60, Duke, serial number P400. The airplane seated six and had a gross weight of 6,775 pounds. The engines were 380 horsepower Lycoming TIO-541-E1C4 engines. The last annual inspection was conducted on September 6, 1996. The airplane had flown 40 hours since the last inspection and had a total time of 3,358 hours.

The engine logbooks indicated that both engines were overhauled on September 30, 1988. The time since overhaul was about 887 hours. The engine teardown revealed that Superior Air Parts pistons (p\n SL 10545) were installed on both engines during the overhaul. The engine teardown revealed that the #3 and #5 pistons in the left engine had SL 10545 Revision AF pistons installed. SL 10545 Revision AF pistons were not produced until February 1990. There were no logbook entries indicating when they had been installed. The #1, #2, and #5 pistons in the right engine had been replaced since overhaul. Logbook entries indicated the dates they had been installed.

The operator of the aircraft reported that they had purchased the airplane in 1996. The operator reported that they did not replace any pistons in the left engine. A logbook entry indicated the operator had replaced the #1 and #5 cylinders on the right engine with chrome reconditioned cylinders on April 1, 1996.

The left engine turbocharger had been replaced on June 30, 1997. Time since replacement was about 3 hours.

The aircraft logbook indicated that maintenance had been performed on the right wing fuel tank on July 10, 1997. The logbook entry read, "Repair fuel seepage right wing by tightening leading edge fuel cell interconnect nipple. Fuel right wing and confirm repair." The aircraft operator reported that fuel had started seeping out of the right wing. To locate the leak, fuel was transferred manually from the right tank to the left tank. The mechanics determined that the fuel was leaking at the interconnect nipple. After the leak was fixed, the fuel in the left tank was pumped back into the right tank utilizing the aircraft's fuel pump and a hose. The operator reported that all...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI97FA220