N5985V

Substantial
None

Piper J3C-65 S/N: 13-640

Accident Details

Date
Sunday, August 3, 1997
NTSB Number
FTW97LA298
Location
CASTLE ROCK, CO
Event ID
20001208X08617
Coordinates
39.370109, -104.849502
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A partial loss of engine power due to a cylinder exhaust valve jammed in the open position from excessive carbon deposits. A factor was the lack of suitable terrain on which to make a forced landing.

Aircraft Information

Registration
Make
PIPER
Serial Number
13-640
Engine Type
Reciprocating
Year Built
1945
Model / ICAO
J3C-65 J3
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
J3C-65

Registered Owner (Current)

Name
LONE STAR FLIGHT MUSEUM
Address
11551 AEROSPACE AVE
City
HOUSTON
State / Zip Code
TX 77034
Country
United States

Analysis

On August 3, 1997, approximately 1030 mountain daylight time, a Piper J3C-65, N5985V, was substantially damaged when it collided with terrain during a forced landing 4 miles south of Castle Rock, Colorado. The private pilot, the only occupant aboard, was not injured. Visual meteorological conditions prevailed, and no flight plan had been filed for the personal flight that was conducted under Title 14 CFR Part 91. The flight originated at Englewood, Colorado, approximately 1000.

According to the pilot, he was in cruise flight at 7,500 feet msl (above mean sea level) when the engine rpm (revolutions per minute) dropped from 2,350 to 1,700. He said that at that altitude, a minimum of 2,150 rpm is required to maintain flight. He configured the airplane for best glide and landed in an open but uneven field. The main landing gear was sheared off and the fuselage buckled.

Postaccident examination disclosed the no. 4 cylinder exhaust valve was stuck open. According to the Teledyne Continental Motors representative who examined the engine, it took "a large hammer to drive the valve out." The valve stem and guide were coated with "gummy black deposits." The pilot, who is an aeronautical engineer and holds an A&P (airframe and powerplant) mechanic's license, said the same situation occurred on July 22, 1995 (see FTW 95-L-A312). Engine examination following that accident revealed the no. 4 cylinder exhaust valve was similarly stuck open, and was attributed to excessive carbon deposits from high octane aviation gasoline usage in a low compression engine.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW97LA298