N87358

Substantial
Minor

Cessna 310R S/N: 0529

Accident Details

Date
Tuesday, December 30, 1997
NTSB Number
FTW98LA081
Location
GRANTS, NM
Event ID
20001208X09315
Coordinates
35.150886, -107.829589
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
3
Total Aboard
4

Probable Cause and Findings

The pilot's failure to maintain adequate airspeed, which resulted in a stall. A factor related to the accident was the pilot's inadequate preflight inspection, which failed to secure the right engine oil cap, resulting in oil exhaustion and the loss of engine power.

Aircraft Information

Registration
Make
CESSNA
Serial Number
0529
Engine Type
Reciprocating
Year Built
1975
Model / ICAO
310R C310
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2
Seats
6
FAA Model
310R

Registered Owner (Current)

Name
BRASWELL EUGENE E III
Address
274 ARNOLD RD
City
LOUISBURG
State / Zip Code
NC 27549-9096
Country
United States

Analysis

On December 30, 1997, at 1100 mountain standard time, a Cessna 310R, N87358, was substantially damaged following landing short of runway 31 at Grants-Milan Municipal Airport, Grants, New Mexico. The private pilot and two of the passengers were not injured; however, a third passenger received minor injuries. The airplane was owned and being operated by the pilot under Title 14 CFR Part 91. Visual meteorological conditions prevailed for the cross-country flight which originated from Los Lunas, New Mexico, approximately 30 minutes before the accident. No flight plan was filed.

According to the pilot, he serviced the right engine with oil prior to departure. While in flight, a passenger reported seeing oil coming from the rear of the right engine. The pilot noticed a rise in oil temperature and a drop in oil pressure. He feathered the right engine; however, the aircraft "was not holding altitude and began to descend at approximately 150 feet per minute. . .and [he] decided to bring the right engine back on line."

When the aircraft was approximately 5 minutes from the Grants-Milan Municipal Airport, the pilot "lower[ed] the landing gear and feather[ed] the propeller, and suddenly the right engine stopped, leaving [him] approximately 100 feet short of the approach end of the runway. [The] aircraft appeared to stall approximately 15 feet above the ground and then dropped suddenly," impacting the ground. It is unknown at what altitude above the ground the pilot lowered the landing gear.

According to the aircraft operating manual, the procedures for a single-engine approach and landing are mixture full rich, propeller full forward, an approach speed of 97 knots, and landing gear down only within glide distance of the field. According to the maximum glide chart, with flaps up, landing gear up, and the propeller of the failed engine feathered, the aircraft should glide 1 nautical mile per 1000 feet.

According to the performance chart for single-engine service ceiling at a maximum gross weight of 5,500 lbs., the aircraft was capable of maintaining an altitude of 7,975 feet, given the temperature of 21 degrees F., the altimeter setting of 30.26 Hg., and an indicated airspeed of 100 knots. The manual does not provide a chart indicating the altitude capability of single-engine operation with the gear down.

Postaccident examination of the aircraft by an FAA inspector revealed that the oil cap was not properly secured on the right engine. As a result, oil was being siphoned from the oil filler tube.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW98LA081