N51258

Substantial
None

Cessna 150J S/N: 15069877

Accident Details

Date
Monday, January 12, 1998
NTSB Number
CHI98LA078
Location
GAYLORD, MI
Event ID
20001211X09406
Coordinates
45.019008, -84.670654
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

the pilot's misjudging the flare leading to a hard landing, and the kit manufacturer's (Supplemental Type Certificate holder's) inadequate design leading to a corrosion stress fracture of the landing gear attachment. A factor was the landing gear attachment corroded.

Aircraft Information

Registration
Make
CESSNA
Serial Number
15069877
Engine Type
Reciprocating
Year Built
1968
Model / ICAO
150J C150
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
150J

Registered Owner (Current)

Name
NELSON OTIS
Address
572 WEST RD
City
PORTAGE
State / Zip Code
ME 04768
Country
United States

Analysis

On January 12, 1998, at 1210 eastern standard time, a ski equipped Cessna 150J, N51258, sustained substantial damage during a hard landing on a snow covered, frozen lake near Gaylord, Michigan. The main landing gear utilized an extension to relocate the axle. That extension fractured and the airplane ground looped. The pilot reported no injuries. The 14 CFR Part 91 personal flight was operating in visual meteorological conditions. No flight plan was on file for the local flight which departed from the Otsego County Airport also near Gaylord, about 1100.

The pilot stated that the right main landing gear extension failed after three landings and on taxi to his hangar. He said that the substantial damage to the airplane occurred at that time.

A witness who talked to the police made a written statement indicating that she watched the airplane make three separate landings and that on the last landing, "Just before it touched down, it kind of hovered sideways and then went almost straight down, bounced back up once and back down and slowly tipped over onto the nose, and one wing."

The fractured landing gear extension was examined by the NTSB's Office of Research and Engineering. Their report No. 98-127 is attached as an addendum to this report. The report indicated that the, "... fracture surfaces showed a majority of fracture features consistent with a failure in overstress." The report indicated that there was a uniformly blackened area on the edge of the surface located at the side of the radius of a cut-out. The blackened area was cleaned and found to be corroded. The corrosion was found in a pattern which appeared to coincide with the outline of the main landing gear leg.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI98LA078