N8SX

Substantial
None

Piper PA-32-300 S/N: 32-754-0015

Accident Details

Date
Tuesday, February 24, 1998
NTSB Number
MIA98LA085
Location
HOLLY SPRINGS, MS
Event ID
20001211X09591
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

a total loss of power due to fuel starvation as a result of the pilot's lack of adequate preflight planning and preparation and his failure to adequately refuel his airplane.

Aircraft Information

Registration
N8SX
Make
PIPER
Serial Number
32-754-0015
Engine Type
Reciprocating
Year Built
1974
Model / ICAO
PA-32-300 PA32
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
92ND WEST AVIATION INC
Address
1423 LINGO RD
Status
Deregistered
City
LONOKE
State / Zip Code
AR 72086-8485
Country
United States

Analysis

On February 24, 1998, about 0715 central standard time, a Piper PA-32-300, N8SX, registered to a private individual, operating as a 14 CFR Part 91 personal flight, crashed on takeoff from Holly Springs/ Marshall County Airport, Holly Springs, Mississippi. Visual meteorological conditions prevailed and no flight plan was filed. The airplane sustained substantial damage, and the private-rated pilot was not injured. The flight was departing at the time of the accident.

The pilot stated he flew N8SX to Holly Springs/Marshall County Airport to visit his father and brother for a few days. He arrived late on the afternoon of February 18, found the FBO closed for the day, so he parked and secured his airplane on their ramp. He returned the next day, requested and watched as N8SX's tip tanks and right main tank were filled, taking on a total of 50.3 gallons. He had resealed the left main fuel cell and wanted that tank dry to "cure" the sealant. On February 23, he had the left main tank fueled with 24.6 gallons in preparation for his trip home early the next morning. Copies of fuelling slips are included in this report under Other Pertinent Forms and Reports.

The pilot stated that immediately after rotation, the engine lost power, and he attempted to land on, "sod between the runway and taxiway," but his momentum carried him beyond the runway environment where he encountered a "two-foot gulley".

An observer at the wreckage site stated the cockpit fuel selector was positioned to the left tip tank detent. The pilot's statement confirms left-tip-tank is the position he had selected. The left tip tank was not compromised and contained about a cup of fuel.

There were no fuel stains under the wings, or on the ramp where the airplane was previously parked. The FBO reports there have been no previous reports of fuel theft from aircraft. The FBO's statements are included in this report under Transcripts of Telephone Communications Pertinent to the Investigation.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA98LA085