N81045

Substantial
None

Cessna 140 S/N: 10335

Accident Details

Date
Monday, September 7, 1998
NTSB Number
ANC98LA140
Location
FAIRBANKS, AK
Event ID
20001211X10973
Coordinates
64.900032, -148.159362
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The loss of engine power due to an in-flight fracture of an engine exhaust valve stem assembly. A factor associated with the accident was the lack of suitable terrain for a forced landing.

Aircraft Information

Registration
N81045
Make
CESSNA
Serial Number
10335
Engine Type
Reciprocating
Year Built
1946
Model / ICAO
140 C140
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
AWBREY MICKEY R
Address
PO BOX 60843
Status
Deregistered
City
FAIRBANKS
State / Zip Code
AK 99706-0843
Country
United States

Analysis

On September 6, 1998, at 1707 Alaska daylight time, a Cessna 140 airplane, N81045, sustained substantial damage when it nosed over during an emergency landing seven miles southeast of the Fairbanks International Airport, Fairbanks, Alaska. The private pilot owner and the sole passenger were not injured. The flight was conducted under 14 CFR Part 91 as a personal flight. The flight departed the Fairbanks/Clear Creek airstrip at 1615, and was returning to Fairbanks International Airport, from a camping trip. Visual meteorological conditions prevailed at the time of the accident, and no flight plan was filed.

The pilot told the NTSB investigator-in-charge during a telephone interview on September 6, and in his NTSB Pilot / Operator report, that while in cruise at 1,500 feet msl, he heard a "clunk" and the engine rpm began to decrease. He stated that application of carburetor heat, and changing fuel tanks did not improve the engine performance. The engine noise continued, and engine rpm continued to decrease. The pilot notified the Fairbanks Air Traffic Control Tower of his emergency, and made a forced landing on tundra. The airplane nosed over during the landing.

Postaccident inspection of the Teledyne Continental Motors C-85-6-12 engine revealed the exhaust valve stem of the number two cylinder had separated, allowing the valve to be ingested into the cylinder. Metal pieces up to 1/2 inch in diameter, were recovered from the cylinder and exhaust manifold. The engine had accumulated 4,555 hours in service at the time of the accident, and 1,089 hours since overhaul.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ANC98LA140