N185Z

Substantial
None

Cessna 185E S/N: 1851363

Accident Details

Date
Monday, November 2, 1998
NTSB Number
LAX99LA021
Location
TUCSON, AZ
Event ID
20001211X11451
Coordinates
32.539890, -110.949798
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

Failure of the pilot to properly secure the seat which subsequently slid back on the takeoff roll and lead to the pilot's loss of aircraft control.

Aircraft Information

Registration
Make
CESSNA
Serial Number
1851363
Engine Type
Reciprocating
Year Built
1968
Model / ICAO
185E C185
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
6
FAA Model
A185E

Registered Owner (Current)

Name
WAB AIR LLC
Address
27 DISCOVERY DR
City
BUTTE
State / Zip Code
MT 59701-3124
Country
United States

Analysis

On November 2, 1998, at 1100 hours mountain standard time, a Cessna 185E, N185Z, ground looped and departed runway 11L on the takeoff roll at the Tucson, Arizona, airport. The aircraft sustained substantial damage. The airline transport pilot, the sole occupant, was not injured. Visual meteorological conditions existed for the personal flight operated under 14 CFR Part 91, and no flight plan was filed.

The pilot reported that as he was on the takeoff roll his seat slid out of the detents. He stated that "this pulled my feet off the rudder pedals and my hands off the controls." The pilot reported that the aircraft made a turn to the left as he was attempting to move the seat forward to regain use of the rudders or the brakes. He reached up to retard the throttle and the aircraft came to a stop after a ground loop. No further mechanical malfunctions were noted with the aircraft.

According to a Federal Aviation Administration (FAA) airworthiness inspector who examined the aircraft at the airport, the seat was stiff and was difficult to move fore and aft. He reported that the detents in the seat rails did not show any signs of wear, and the pilot may have thought he had the seat locked into place because of the stiffness of the seat. The FAA did note that the aircraft was 40 hours out of annual, but that the condition of the seat and seat rails would have passed an annual inspection.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX99LA021