N8086P

Substantial
Minor

Piper PA-24-250 S/N: 24-3334

Accident Details

Date
Saturday, December 5, 1998
NTSB Number
LAX99LA044
Location
VICTORVILLE, CA
Event ID
20001211X11578
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

Fuel starvation caused by the pilot's failure to select a tank containing fuel.

Aircraft Information

Registration
N8086P
Make
PIPER
Serial Number
24-3334
Engine Type
Reciprocating
Model / ICAO
PA-24-250 PA24
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
CATES THOMAS M
Address
19143 OTILLA
Status
Deregistered
City
BLOOMINGTON
State / Zip Code
CA 92316
Country
United States

Analysis

On December 5, 1998, at 1056 hours Pacific standard time, a Piper PA-24-250, N8086P, collided with ground obstructions during a forced landing 2.5 miles north of the Southern California International Airport, Victorville, California. The forced landing was precipitated by a total loss of engine power during a practice instrument approach to the airport. Visual meteorological conditions prevailed at the time. The aircraft, owned and operated by the pilot under 14 CFR Part 91, sustained substantial damage. The private pilot, the sole occupant, incurred minor injuries. The flight originated from the Rialto, California, airport, with a planned stop at Apple Valley, California. The pilot departed Apple Valley Airport at 1045, and intended to practice instrument approaches at the Southern California Airport, prior to returning to Rialto.

An officer from the San Bernardino Sheriff's Department interviewed the pilot after the accident. The pilot stated that before he took off from Rialto Airport, he preflighted the aircraft and found that one tank was a little low on fuel, and the other tanks were full. There were no discrepancies with the flight from Rialto to Apple Valley. After a brief stop, the pilot proceeded to Southern California International to practice ILS approaches; he was on a 10 to 15 mile DME arc when the engine stopped. The pilot stated he applied carburetor heat and switched fuel tanks; however, the engine did not restart prior to ground contact.

The responding Sheriff's deputy examined the aircraft visually and found no evidence of fuel system leaks.

Aircraft Recovery Services of Compton, California recovered the aircraft and reported that the right main fuel tank was empty. The right outboard left main, and left outboard tanks were full. The fuel selector valve was on the right main fuel tank. The fuel system was inspected and found to be continuous and there were no leaks.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX99LA044