N86SDMITSUBISHI MU-2B-60 1993-04-19 NTSB Accident Report

Destroyed
Fatal

MITSUBISHI MU-2B-60 S/N: 765 S.A.

Summary

On April 19, 1993, a Mitsubishi MU-2B-60 (N86SD) was involved in an accident near Zwingle, IA. The accident resulted in 8 fatal injuries. The aircraft was destroyed.

The National Transportation Safety Board determined the probable cause of this accident to be: THE FATIGUE CRACKING AND FRACTURE OF THE PROPELLER HUB ARM. THE RESULTANT SEPARATION OF THE HUB ARM AND THE PROPELLER BLADE DAMAGED THE ENGINE, NACELLE, WING, AND FUSELAGE, THEREBY CAUSING SIGNIFICANT DEGRADATION TO AIRCRAFT PERFORMANCE AND CONTROL THAT MADE A SUCCESSFUL LANDING PROBLEMATIC. THE CAUSE OF THE PROPELLER HUB ARM FRACTURE WAS A REDUCTION IN THE FATIGUE STRENGTH OF THE MATERIAL BECAUSE OF MANUFACTURING AND TIME-RELATED FACTORS (DECARBURIZATION, RESIDUAL STRESS, CORROSION, MIXED MICROSTRUCTURE, AND MACHINING/SCORING MARKS) THAT REDUCED THE FATIGUE RESISTANCE OF THE MATERIAL, PROBABLY COMBINED WITH EXPOSURE TO HIGHER-THAN-NORMAL CYCLIC LOADS DURING OPERATION OF THE PROPELLER AT A CRITICAL VIBRATION FREQUENCY (REACTIONLESS MODE), WHICH WAS NOT APPROPRIATELY CONSIDERED DURING THE AIRPLANE/PROPELLER CERTIFICATION PROCESS.

This accident is documented in NTSB report DCA93GA042. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N86SD.

Accident Details

Date
Monday, April 19, 1993
NTSB Number
DCA93GA042
Location
ZWINGLE, IA
Event ID
20001211X12106
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
8
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
8

Probable Cause and Findings

THE FATIGUE CRACKING AND FRACTURE OF THE PROPELLER HUB ARM. THE RESULTANT SEPARATION OF THE HUB ARM AND THE PROPELLER BLADE DAMAGED THE ENGINE, NACELLE, WING, AND FUSELAGE, THEREBY CAUSING SIGNIFICANT DEGRADATION TO AIRCRAFT PERFORMANCE AND CONTROL THAT MADE A SUCCESSFUL LANDING PROBLEMATIC. THE CAUSE OF THE PROPELLER HUB ARM FRACTURE WAS A REDUCTION IN THE FATIGUE STRENGTH OF THE MATERIAL BECAUSE OF MANUFACTURING AND TIME-RELATED FACTORS (DECARBURIZATION, RESIDUAL STRESS, CORROSION, MIXED MICROSTRUCTURE, AND MACHINING/SCORING MARKS) THAT REDUCED THE FATIGUE RESISTANCE OF THE MATERIAL, PROBABLY COMBINED WITH EXPOSURE TO HIGHER-THAN-NORMAL CYCLIC LOADS DURING OPERATION OF THE PROPELLER AT A CRITICAL VIBRATION FREQUENCY (REACTIONLESS MODE), WHICH WAS NOT APPROPRIATELY CONSIDERED DURING THE AIRPLANE/PROPELLER CERTIFICATION PROCESS.

Aircraft Information

Registration
Make
MITSUBISHI
Serial Number
765 S.A.
Engine Type
Turbo-shaft
Model / ICAO
MU-2B-60 MU2
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
SOUTH DAKOTA STATE OF
Address
TRANSPORTATION BUILDING
Status
Deregistered
City
PIERRE
State / Zip Code
SD 57501
Country
United States

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DCA93GA042