N66155

Substantial
None

CESSNA 150M S/N: 15075878

Accident Details

Date
Saturday, July 24, 1993
NTSB Number
CHI93LA279
Location
BRIDGMAN, MI
Event ID
20001211X12862
Coordinates
41.939960, -86.560142
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

the pilot's premature lift-off.

Aircraft Information

Registration
N66155
Make
CESSNA
Serial Number
15075878
Engine Type
Reciprocating
Year Built
1974
Model / ICAO
150M C150
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
276 ROUTE 206
Status
Deregistered
City
ANDOVER
State / Zip Code
NJ 07821
Country
United States

Analysis

On July 24, 1993, about 1430 eastern daylight time, a Cessna 150M airplane, N66155, sustained substantial damage during an attempted takeoff from Hitchcock Field, Bridgman, Michigan. The private pilot and sole passenger aboard were not injured. The flight operated in visual meteorological conditions under 14 CFR Part 91.

The pilot reported he was attempting to takeoff from runway 22, an 1,800' turf strip. He estimated the wind was from approximately 165 degrees at 3-5 knots. The pilot's Pilot/Operator Accident Report states, in part: "I proceeded to far end of runway (NE) for run-up ...then proceeded to take-off under full power. Rotation was achieved prior to mid-field intersection, with lift-off at intersection. Nose was levelled to accumulate more speed. Aircraft was approx. 4-6 feet agl, minimal additional speed was achieved over next 6-8 seconds. During this period, threshold was already getting close, with row of bushes and saplings displaced approx. 15-20 beyond threshold. These ranged in height from approx. 8-20 feet... . With airspeed at around 55 I determined aircraft could neither land straight-on nor clear this varied height obstacles. As I attempted to utilize the "dog-leg right" rough field, the right wing dropped/hit from lack of sufficient power to adjust."

The pilot claimed no mechanical failure or malfunction in his report to the NTSB.

A telephone interview was conducted with the pilot on September 20, 1993. The pilot recounted the airplane felt sluggish in accelerating, but was developing maximum RPM of 2700. He said the throttle was pushed all the way forward, but stopped approximately one to one and one-half inches from the panel.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI93LA279