N8962L

Substantial
Minor

GRUMMAN AA-1B S/N: AA1B-0412

Accident Details

Date
Sunday, July 4, 1993
NTSB Number
MIA93LA149
Location
OCALA, FL
Event ID
20001211X12980
Coordinates
29.159351, -82.209068
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

PREMATURE LIFT OFF BY THE PILOT DURING TAKEOFF.

Aircraft Information

Registration
N8962L
Make
GRUMMAN
Serial Number
AA1B-0412
Engine Type
Turbo-shaft
Model / ICAO
AA-1B V1
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
HINES WILLIAM JR
Address
301 OAK TRACK TRAIL
Status
Deregistered
City
OCALA
State / Zip Code
FL 34472
Country
United States

Analysis

On July 4, 1993, about 0906 eastern daylight time, a Grumman AA-1B, N8962L, registered to the pilot, William L. Hines, was substantially damaged during an aborted takeoff from the Ocala Municipal Airport, Ocala, Florida, while on a 14 CFR Part 91 personal flight. Visual meteorological conditions prevailed at the time and no flight plan was filed for the local flight. The private pilot sustained minor injuries. The flight was originating at the time of the accident.

The pilot stated that during the initial climb, the aircraft shuddered as if it would fall apart. The shuddering stopped after he decreased the angle of attack; and the engine did respond to throttle input. He again initiated a climb and the shuddering began again. He aborted the takeoff and while maneuvering to avoid obstacles at the departure end of the runway, the airplane stalled and landed hard on grass. The nose and right main landing gears collapsed. He further stated that the shuddering was similar to that encountered when performing stalls and that he did not hear any unusual engine sounds.

As a result of the accident, the fuel tanks were damaged but the remaining fuel in them, the carburetor, and electric fuel pump were checked for water; none was found. A slight amount of sediment was found. An A & P mechanic who examined the engine stated that it was "intact." The magnetos were removed, rotated by hand, which revealed that they produced more than sufficient spark.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA93LA149