Summary
On August 01, 1993, a Cessna 150M (N66081) was involved in an incident near Bald Knob, AR. All 1 person aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: FUEL EXHAUSTION DUE TO THE PILOT'S FAILURE TO REFUEL. A FACTOR WAS THE LACK OF SUITABLE TERRAIN FOR THE FORCED LANDING.
On August 1, 1993, at approximately 0915 central daylight time, a Cessna 150M, N66081, sustained substantial damage near Bald Knob, Arkansas, during a forced landing following a loss of engine power. The private pilot was not injured. Visual meteorological conditions prevailed for the personal cross country flight.
During interviews, conducted by a Federal Aviation Administration (FAA) inspector, with the pilot the following information was revealed. The pilot departed Lexington, Mississippi, at 0710 after adding ten gallons of fuel for the planned two hour flight to Batesville, Arkansas. Approximately 20 minutes from the destination, the engine lost power. A forced landing was initiated to a field.
This incident is documented in NTSB report FTW93LA224. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N66081.
Accident Details
Probable Cause and Findings
FUEL EXHAUSTION DUE TO THE PILOT'S FAILURE TO REFUEL. A FACTOR WAS THE LACK OF SUITABLE TERRAIN FOR THE FORCED LANDING.
Aircraft Information
Registered Owner (Historical)
Analysis
On August 1, 1993, at approximately 0915 central daylight time, a Cessna 150M, N66081, sustained substantial damage near Bald Knob, Arkansas, during a forced landing following a loss of engine power. The private pilot was not injured. Visual meteorological conditions prevailed for the personal cross country flight.
During interviews, conducted by a Federal Aviation Administration (FAA) inspector, with the pilot the following information was revealed. The pilot departed Lexington, Mississippi, at 0710 after adding ten gallons of fuel for the planned two hour flight to Batesville, Arkansas. Approximately 20 minutes from the destination, the engine lost power. A forced landing was initiated to a field. During the landing roll, the nose gear collapsed when it hit a hole in the uneven terrain.
The Pilot/Operator report submitted to the Safety Board, revealed that fuel on board at departure was 19 gallons.
During an on site examination of the fuel system by a FAA inspector, the fuel tank integrity had not been compromised and no fuel was found in the left fuel tank and less than one gallon was found in the right fuel tank.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW93LA224