N23192

Substantial
Serious

CESSNA 150H S/N: 15068784

Accident Details

Date
Saturday, September 4, 1993
NTSB Number
FTW93LA253
Location
WEATHERFORD, TX
Event ID
20001211X13399
Coordinates
32.750614, -97.770332
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

FUEL EXHAUSTION. FACTORS WERE: THE PILOT'S FAILURE TO HAVE THE AIRPLANE SERVICED TO CAPACITY PRIOR TO DEPARTURE, AND HIS ERRONEOUS FUEL CONSUMPTION CALCULATIONS.

Aircraft Information

Registration
N23192
Make
CESSNA
Serial Number
15068784
Engine Type
Reciprocating
Year Built
1968
Model / ICAO
150H C150
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
CARLTON CHRISTOPHER C
Address
1604 BRUNSON CT
Status
Deregistered
City
ARLINGTON
State / Zip Code
TX 76012
Country
United States

Analysis

On September 4, 1993, at approximately 1348 central daylight time, the pilot of a Cessna 150H, N23192, made a forced landing near Weatherford, Texas, after the engine lost power. The solo private pilot sustained serious injuries, and the airplane was substantially damaged. Visual meteorological conditions prevailed at the time, and no flight plan was filed for the personal flight.

The following is based on information collected by the Federal Aviation Administration FAA). The pilot departed Northwest Regional Airport, Fort Worth, Texas, on a proposed cross country flight to Ranger, Texas. The pilot told an FAA inspector that he was unable to locate Ranger Airport, so he turned around and was returning to Fort Worth when the engine lost power. The pilot indicated on his accident report that both fuel gauges registered 1/4 full. Witnesses reported seeing the airplane lose altitude and said the engine was not operating. The FAA inspector reported the fuel tanks were not compromised, no fuel was found in the tanks, and no fuel stains were noted on the ground.

On September 8, 1993, the engine was examined by representatives of the Federal Aviation Administration, Cessna Aircraft Company, and Teledyne Continental Motors. The following is based on a report submitted by the Cessna Aircraft Company. Drive train continuity was established and all four cylinders had compression. The top spark plugs were dry. Only a few drops of fuel was noted in the carburetor bowl. Two ounces of fuel was drained from the gascolator. Salvage personnel reported there was about 1/2 gallon of fuel in the left tank and about one gallon of fuel in the right tank.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW93LA253