N731UF

Substantial
None

CESSNA A188B S/N: 18803160T

Accident Details

Date
Sunday, September 19, 1993
NTSB Number
FTW93LA260
Location
MANILA, AR
Event ID
20001211X13404
Coordinates
35.879394, -90.160728
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

PARTIAL LOSS OF ENGINE POWER DUE TO THE COLLAPSE OF AN AIR INDUCTION HOSE.

Aircraft Information

Registration
Make
CESSNA
Serial Number
18803160T
Engine Type
Reciprocating
Year Built
1978
Model / ICAO
A188B C188
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
1
FAA Model
A188B

Registered Owner (Current)

Name
PENISTON BOB
Address
11788 LIV 519
City
CHILLICOTHE
State / Zip Code
MO 64601-8384
Country
United States

Analysis

On September 19, 1993, at 1415 central daylight time, a Cessna A188B, N731UF, sustained substantial damage following a partial loss of engine power during takeoff near Manila, Arkansas. The commercial pilot was not injured. Visual meteorological conditions prevailed for the local aerial application flight.

The pilot stated on the enclosed Pilot/Operator report, and during interviews conducted by a Federal Aviation Administration inspector, that the airplane was loaded with 1,600 pounds of cotton defoliate and that this was the twelfth load of the day. He further stated that this takeoff took much longer than the others. When the tail came up, he had forward visibility and he observed the remaining runway was marginal for a safe takeoff; however, "an abort was not safe because of a ditch at the end of the runway." The pilot continued the takeoff and began dumping the load at the last 200 feet of the runway. The airplane lifted off the runway at 100 feet before the end of the runway; however, it would not accelerate and began descending. At approximately 300 feet off the end of the runway, the pilot shut down the engine, as the spray booms caught in the cotton, and the airplane was pulled to the left and subsequently hit the ground.

Examination of the double wall air induction hose by the operator revealed that the inside wall had separated and was blocking the air flow.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW93LA260