N9000M

Substantial
None

PIPER PA-32-300 S/N: 32-7240053

Accident Details

Date
Sunday, November 7, 1993
NTSB Number
MIA94LA017
Location
PLYMOUTH, FL
Event ID
20001211X13778
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

TOTAL FAILURE OF THE CRANKSHAFT DUE TO FATIGUE RESULTING IN A FORCED LANDING AND SUBSEQUENT HARD LANDING.

Aircraft Information

Registration
Make
PIPER
Serial Number
32-7240053
Engine Type
Reciprocating
Year Built
1971
Model / ICAO
PA-32-300 PA32
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
6
FAA Model
PA-32-300

Registered Owner (Current)

Name
SAIPAN TRANSPORTATION MANAGEMENT SOLUTIONS INC
Address
PO BOX 500150
City
SAIPAN
State / Zip Code
MP 96950-0150
Country
United States

Analysis

On November 7, 1993, about 1500 eastern standard time, a Piper PA-32-300, N9000M, registered to Thomas J. and Carol A. Lewis, was substantially damaged during a forced landing about 5 miles north of Plymouth, Florida, while on a 14 CFR Part 91 personal flight. Visual meteorological conditions prevailed at the time and no flight plan was filed. The private-rated pilot, the sole occupant, was not injured. The flight originated about 10 minutes earlier from the Orlando Country Airport, Plymouth, Florida.

The pilot stated that shortly after takeoff while climbing to cruise, the engine began losing power, then failed. He initiated an emergency descent and while attempting a forced landing in a field, the airplane landed hard and collided with fence poles.

The engine was removed for further examination by the manufacturer and an FAA airworthiness inspector. Examination of the engine revealed that the crankshaft failed at the connecting rod thrust face just above the rear fillet radius of the No.5 crankpin journal. Dimensional measurements of all journals revealed that they were within the overhaul manual service limits. Chemical analysis revealed that the crankshaft material conformed to specification requirements. The case depth, case hardness, and core hardness of the crankshaft were determined to conform to the engineering drawing requirements.

Metallurgical examination of the fracture surfaces by the engine manufacturer revealed that the crankshaft failed due to fatigue. Magnetic particle inspection revealed heat cracks at all of the connecting rod thrust faces just above the front as well as rear fillet radii of the crankpin journals. Additionally, severely damaged spots were observed at the crank cheeks and some damaged areas were blended with no nitriding case observed in the blended areas. The metallurgical report states that lack of concaveness of the beach mark patterns at the apparent origin indicate that the fatigue initiated from a surface origin.

Review of the engine logbook revealed that the engine was major overhauled on July 27, 1990, and about 1 hour later during the engine break-in period, a camshaft follower failed. The engine was disassembled and the crankshaft in part was sent to an FAA approved repair station where the crankshaft was magnafluxed. According to the repair station work order, no cracks were detected. The crankshaft was returned and several components of the engine was replaced including both halves of the crankcase. The engine was overhauled, installed, and at the time of the accident had accumulated about 372.07 hours since the second overhaul.

The manufacturer's metallurgical report was reviewed by personnel in the NTSB Materials Laboratory in Washington, D.C., who state that the report adequately documents the factual observations.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA94LA017