N2567K

Substantial
None

Cessna 180K S/N: 18052990

Accident Details

Date
Sunday, May 23, 1999
NTSB Number
SEA99LA073
Location
BREMERTON, WA
Event ID
20001212X18897
Coordinates
47.570384, -122.630149
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

Failure of the landing gear attach bolt due to fatigue failure resulting in the left main landing gear collapsing.

Aircraft Information

Registration
Make
CESSNA
Serial Number
18052990
Engine Type
Reciprocating
Year Built
1978
Model / ICAO
180K C180
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
180K

Registered Owner (Current)

Name
BRYANT KENNETH D
Address
25022 ROBERTS DR
City
BLACK DIAMOND
State / Zip Code
WA 98010-9212
Country
United States

Analysis

On May 23, 1999, approximately 1535 Pacific daylight time, a Cessna 180K, N2567K, impacted the runway at Bremerton National Airport, Bremerton, Washington, after the failure of a main gear leg during the landing roll. The private pilot, who was the operator of the aircraft, was not injured, but the aircraft sustained substantial damage. The 14 CFR Part 91 flight, which departed Crest Airpark, Covington, Washington, about 30 minutes earlier, was being operated in visual meteorological conditions. No flight plan had been filed, and there was no report of an ELT activation.

According to the pilot, who was performing a wheel landing, the touchdown was normal. But as the landing roll continued, he lost control of the aircraft when the left main gear leg failed. Immediately after the gear failed, the aircraft settled onto the runway and slid to a stop.

Post-accident inspection revealed that the attachment bolt from the gear leg broke in two pieces. The bolt was sent to the National Transportation Safety Board Materials Laboratory, Washington D.C. for examination. The specialist reported that "the bolt separated at the edge of the self-locking nut, through the first thread on the shank." Further examination with the aid of a low-power binocular microscope revealed three major fracture zones. The specialist reported that two of the zones were "fairly flat and propagated on a plane that was roughly perpendicular to the bolt axis, typical of fatigue progression." One of the zones was covered with heavy accumulation of oxides and corrosion deposits. The other zone was free of oxidation and deposits. The third zone displayed a fracture propagation on a slant (45 degree) plane. The specialist reported this zone as "typical of a final overstress separation." The specialist reported that "the fatigue occupied approximately 75 percent of the bolt cross section at the fracture location." The specialist also reported that the presence of oxide and corrosion deposits suggest an "old crack." There was no evidence found of thread stripping.

The aircraft was purchased new in 1978. The aircraft maintenance logbooks indicate that that the aircraft had accumulated about 38 hours of total time at the annual inspection performed in March of 1981. The next annual inspection was signed off in June 1995, with a total time still indicating 38 hours. In February 1999, the logbook indicated an annual inspection with a total time of 69.5 hours accumulated. The pilot reported a total aircraft time of 77 hours at the time of the accident.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA99LA073