N2651N

Substantial
None

Cessna 120 S/N: 12909

Accident Details

Date
Friday, June 25, 1999
NTSB Number
LAX99LA227
Location
CHINO, CA
Event ID
20001212X19037
Coordinates
33.999576, -117.679924
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A preexisting fatigue fracture of the right axle.

Aircraft Information

Registration
N2651N
Make
CESSNA
Serial Number
12909
Engine Type
Reciprocating
Year Built
1947
Model / ICAO
120 C120
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
STOKES MICHAEL J
Address
120 S CRAIG AVE APT 1
Status
Deregistered
City
PASADENA
State / Zip Code
CA 91107-4000
Country
United States

Analysis

On June 24, 1999, at 1808 hours Pacific daylight time, a Cessna 120, N2651N, ground looped and collapsed the right landing gear during a touch-and-go landing at the Chino, California, airport. The airplane, owned and operated by the student pilot under 14 CFR Part 91, sustained substantial damage. The pilot was not injured during the local area solo instructional flight. Visual meteorological conditions existed for the flight and no flight plan was filed. The flight had originated at the Chino airport at 1730.

The pilot stated that on the landing rollout the airplane veered to the left. He applied right rudder, which did not correct the travel to the left. He engaged the right brake, which did not have an effect on the airplane's movement to the left. The pilot reported that he was unable to perform a go-around due to the airplane's direction of travel. He kept the airplane on the asphalt, with the wings level, and applied the brakes to stop the airplane. He stated that the airplane "executed a moderate 180 [degree] turn," and the right wheel broke free. The right landing gear spar dug into the asphalt and broke free, the airplane made a turn to the right and the right wing struck the ground.

A Safety Board investigator examined the right main landing gear and noted the appearance of a crack in the right axle. The axle was sent to the Safety Board's metallurgical laboratory for examination. The examination revealed that the fracture was through the barrel near the mounting flange. A microscopic examination of the fracture faces showed a discolored crescent-shaped area consistent with a preexisting crack. A stereo microscopic examination revealed that the crescent region had fracture features typical of multiple origin fatigue cracking. The scanning electron microscope examinations on the mounting flange fracture revealed optical observations of fatigue and overstress. The examination revealed fatigue striations and ductile dimples respectively. It was also noted that a crack existed diametrically opposite of the fatigue crescent. It was also examined and found to have characteristics similar to the original fracture crescent.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX99LA227