N7660U

Substantial
None

Cessna 150M S/N: 150-77786

Accident Details

Date
Wednesday, July 7, 1999
NTSB Number
FTW99LA185
Location
POCAHONTAS, AR
Event ID
20001212X19266
Coordinates
36.260704, -90.959030
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The failure of the carburetor heat control cable which resulted in a partial loss of engine power during initial takeoff climb. A factor was the lack of suitable terrain for the forced landing.

Aircraft Information

Registration
N7660U
Make
CESSNA
Serial Number
150-77786
Engine Type
Reciprocating
Year Built
1976
Model / ICAO
150M C150
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
2825 13TH AVE S
Status
Deregistered
City
MINNEAPOLIS
State / Zip Code
MN 55407-1417
Country
United States

Analysis

On July 7, 1999, at 1400 central daylight time, a Cessna 150M airplane, N7660U, was substantially damaged during a forced landing following a partial loss of engine power during takeoff from the Nick Wilson Field Airport, near Pocahontas, Arkansas. The flight instructor and the student pilot receiving instruction were not injured. The airplane was registered to and operated by the flight instructor, who was doing business as Swink Aviation of Pocahontas, Arkansas. Visual meteorological conditions prevailed for the Title 14 CFR Part 91 local flight for which a flight plan was not filed. The instructional flight originated from the same location approximately 20 minutes prior to the accident.

The 3,765-hour flight instructor reported that the student pilot receiving instruction had accumulated a total of 5 flight hours. The flight instructor elected to stay in closed traffic at the Nick Wilson Field Airport (M70), to practice takeoffs and landings. During the fifth takeoff of the afternoon, a partial loss of engine power occurred during initial takeoff climb from runway 36. The flight instructor stated that, suspecting carburetor ice, he pulled the carburetor heat lever to the full hot (out) position, and the knob, with a portion of the control cable still attached, came all the way out.

The flight instructor stated that he assumed the controls. He added that the power available was not sufficient to maintain a climb rate. The flight instructor maneuvered the airplane to avoid trees and obstacles until he was able to execute a forced landing to an open field. During the landing roll in the soft dirt, the airplane nosed over and came to rest in the inverted position approximately 1/4 mile from the departure end of runway 36.

Examination of the airplane by the flight instructor revealed that the fuselage, aft of the baggage compartment, sustained structural damage. Examination of the carburetor heat control cable confirmed that the control cable was fractured, and the carburetor heat lever was found in the full "on" position. Based on the physical appearance of the control cable, the flight instructor suspected that the cable was "original equipment." A review of the maintenance records by the FAA inspector revealed that the airplane had accumulated a total of 6,837 flight hours since new.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW99LA185