N3755V

Substantial
None

Cessna 150M S/N: 15076611

Accident Details

Date
Friday, August 6, 1999
NTSB Number
CHI99LA277
Location
SIKESTON, MO
Event ID
20001212X19434
Coordinates
36.880786, -89.580688
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

the loss of engine power due to the stuck exhaust valve. A factor was the lack of suitable terrain available for the forced landing.

Aircraft Information

Registration
N3755V
Make
CESSNA
Serial Number
15076611
Engine Type
Reciprocating
Year Built
1975
Model / ICAO
150M C150
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
JOLLIFF PERRY
Address
8 MONA DR
Status
Deregistered
City
SIKESTON
State / Zip Code
MO 63801
Country
United States

Analysis

On August 6, 1999, at 1530 central daylight time, a Cessna 150M, N3755V, operated by Jolliff Aviation was substantially damaged when it experienced a loss of engine power on takeoff and nosed over in a soft field after a forced landing. The 14 CFR Part 91 flight had departed Sikeston Memorial Airport, Sikeston, Missouri, on a local instructional flight. The Certified Flight Instructor (CFI) and student pilot were not injured. Visual meteorological conditions prevailed and no flight plan was filed.

The CFI reported that the engine was operating normally during run-up and takeoff. He reported that at about 200 feet above ground altitude, the engine started running rough. He applied carburetor heat and nosed the airplane over to maintain airspeed. The airplane continued to descend even though the pilot had applied full power. The CFI decided to land the airplane in a field at the end of the runway. He used full flaps and landed the airplane in the soft field. The airplane nosed over during landing rollout.

An inspection of the engine revealed that one of the cylinders had an exhaust valve stuck in the open position. The owner and operator of the airplane reported that during the last 100 hour inspection, the cylinder with the stuck valve had a compression reading of 68 psi, just slightly lower than the other three cylinders.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI99LA277