N735BS

Substantial
None

William John Schulz WJS JAYBIRD S/N: 001

Accident Details

Date
Tuesday, August 10, 1999
NTSB Number
MIA99LA228
Location
TANGERINE, FL
Event ID
20001212X19595
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

the pilot's improper torqueing of a rocker arm adjusting jam nut, that resulted in the adjuster loosening, and a partial loss of engine power. This resulted in the pilot making an off airport precautionary landing and subsequent nose over, during which the aircraft received substantial damage.

Aircraft Information

Registration
Make
WILLIAM JOHN SCHULZ
Serial Number
001
Engine Type
Reciprocating
Year Built
1999
Model / ICAO
WJS JAYBIRD FEST
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
1
FAA Model
WJS JAYBIRD

Registered Owner (Current)

Name
RANCHLANDS
Address
22500 S PEYTON HWY
City
COLORADO SPRINGS
State / Zip Code
CO 80928-9483
Country
United States

Analysis

On August 10, 1999, about 1420 eastern daylight time, a William John Schulz WJS Jaybird, N735BS, registered to a private owner, operated as a 14 CFR Part 91 personal flight, crashed while attempting a precautionary landing in an open field in Tangerine, Florida. Visual meteorological conditions prevailed, and no flight plan was filed. The airplane was substantially damaged, and the private-rated pilot was not injured. The flight originated from Bob White Field, Zellwood, Florida, about 1400, the same day.

The pilot stated that he was en route to Mid Florida Airport, Eustis, Florida, when a partial power loss and the inability to hold altitude necessitated a precautionary landing on a mowed lawn. The pilot said he executed a landing with a left quartering tailwind, due to utility lines and trees blocking an approach into the wind. The aircraft bounced, and on the second bounce the right landing gear bent and the wind lifted the left wing. The aircraft slid, and slowly nosed over, coming to rest upside down. The pilot further stated that the reason for engine power loss was due to his improper maintenance/installation by not having sufficient torque on the jam nut exhaust valve adjuster (rocker arm) to number 4 cylinder.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA99LA228