Summary
On October 20, 1999, a Piper PA-24-250 (N8078P) was involved in an accident near Bozeman, MT. The accident resulted in 2 minor injuries. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this accident to be: The pilot-in-command's (CFI) failure to take remedial action. Factors include the private pilot letting the airspeed get too low.
On October 20, 1999, approximately 1000 mountain daylight time, a Piper PA-24-250, N8078P, experienced a hard landing during a simulated engine-out approach at Gallatin Field, Bozeman, Montana. The flight instructor and the private pilot received minor injuries, and the aircraft, which was owned and operated by the private pilot, sustained substantial damage. The local 14 CFR Part 91 instructional flight, which began about 60 minutes prior to the accident, was being conducted in visual meteorological conditions. No flight plan had been filed, and there was no report of an ELT activation.
According to an FAA Inspector from the Helena FSDO, the private pilot's flight review was not current, and this was an instructional flight which he hoped would be the basis for renewing his review.
This accident is documented in NTSB report SEA00LA006. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N8078P.
Accident Details
Probable Cause and Findings
The pilot-in-command's (CFI) failure to take remedial action. Factors include the private pilot letting the airspeed get too low.
Aircraft Information
Registered Owner (Current)
Analysis
On October 20, 1999, approximately 1000 mountain daylight time, a Piper PA-24-250, N8078P, experienced a hard landing during a simulated engine-out approach at Gallatin Field, Bozeman, Montana. The flight instructor and the private pilot received minor injuries, and the aircraft, which was owned and operated by the private pilot, sustained substantial damage. The local 14 CFR Part 91 instructional flight, which began about 60 minutes prior to the accident, was being conducted in visual meteorological conditions. No flight plan had been filed, and there was no report of an ELT activation.
According to an FAA Inspector from the Helena FSDO, the private pilot's flight review was not current, and this was an instructional flight which he hoped would be the basis for renewing his review. The inspector said that during the review, the flight instructor reduced the engine power in order to simulate an engine failure, and then instructed the private pilot to land the aircraft. According to the private pilot, he tried to "stretch" the glide in order to reach the end of the runway, but the airspeed began to slow, and the aircraft dropped in hard just after crossing the runway threshold. Although the airspeed had slowed below normal approach speed as the aircraft neared the approach end of the runway, the instructor pilot did not attempt to add power, nor did she call for termination of the simulated forced landing exercise.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA00LA006