N7878P

Substantial
Serious

Piper PA-24-250 S/N: 24-3104

Accident Details

Date
Sunday, February 13, 2000
NTSB Number
FTW00LA081
Location
COLLEGE STATION, TX
Event ID
20001212X20488
Coordinates
30.599802, -96.309356
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
2
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The loss of engine power due to fuel system contamination. A factor was the lack of suitable terrain for the forced landing.

Aircraft Information

Registration
N7878P
Make
PIPER
Serial Number
24-3104
Engine Type
Reciprocating
Year Built
1962
Model / ICAO
PA-24-250 PA24
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
WHITE INDUSTRIES INC
Address
PO BOX 198
Status
Deregistered
City
BATES CITY
State / Zip Code
MO 64011-0198
Country
United States

Analysis

On February 13, 2000, at 1630 central standard time, a Piper PA-24-250, single-engine airplane, N7878P, sustained substantial damage when it impacted the terrain short of the runway following a loss of engine power. The private pilot, who owned and operated the airplane under 14 Code of Federal Regulations Part 91, and his passenger received serious injuries. Visual meteorological conditions prevailed for the personal cross-country flight, which departed Conroe, Texas, at 1600. A flight plan was not filed.

During personal telephone interviews, conducted by the NTSB investigator-in-charge (IIC), with local authorities, air traffic control personnel, the FAA inspector, and the pilot, the following information was revealed. The airplane cruised en route from Conroe, Texas, to College Station, Texas, at 4,500 feet msl. Approximately 15 miles from the Easterwood Field Airport, near College Station, the pilot was cleared to land the airplane on runway 28. On a 1.4 nautical mile final approach the engine "stopped." The pilot "immediately switched [the] fuel tank [and] checked fuel pump on." There was "no response from the engine." Upon realizing that the current glidepath would put the airplane into trees, the pilot decided to land in a field short of the trees. Once the airplane was on the ground, the pilot secured the cockpit, released his seat belt, exited the airplane through the cockpit door, and awaited assistance from local authorities.

A review of the pilot records revealed that the private pilot held airplane single-engine land and instrument ratings. He was issued a third class medical certificate on February 24, 1999. On the Pilot/Operator Aircraft Accident Report (NTSB Form 6120.1/2) the pilot reported a total accumulated flight time of 510.7 hours of which 260.7 hours were in the make and model of the accident aircraft.

The FAA inspector responding to the site, which was approximately 1 mile east of the approach end of runway 28, found structural damage to the right wing spar, firewall, and engine mounts. The main landing gear and propeller sustained damage.

On April 25, 2000, the airplane was examined at Lancaster, Texas, under the supervision of a FAA inspector. Continuity of the fuel system was confirmed. The FAA inspector reported finding contamination (ferrous and nonferrous) in the fuel system. The fuel selector valve was examined and there was a "line of corrosion present that extended to the top of the bowl, and caused corrosion on the selector valve housing above the fuel strainer. This indicates that at one time a great deal of water had been present in the selector valve." The electric pumps were examined and there was "evidence of corrosion debris in the bowl of these pumps, indicating that there had been water present in the electric pumps." The fuel pump strainer was removed, and "there was a great deal of debris in the strainer, as well as external to the strainer housing." The inspector stated that "the presence of contamination beyond the strainer indicates that the strainer did not contain all the contaminants." There was a "great deal of corrosion [found] in the L/H [left hand] wing, outboard cavity."

During an engine run at 2,450 rpm, the fuel pressure dropped to less than 1 PSI. However, the engine ran with "no apparent anomalies."

Following the engine run, the carburetor was disassembled. There was debris in the float bowl "consistent with the contamination found throughout the fuel system." The FAA inspector stated "it is obvious from the inspection of the aircraft fuel system that this aircraft has had a water contamination and deterioration of the fuel system."

The engine (Textron Lycoming) representative reported that the carburetor float valve was not attached to the float valve clip on the float and lever assembly. Therefore, the "float valve would not be opened by the float when the fuel lever in the carburetor bowl went down. The float valve would then have to be opened by fuel pressure and gravity."

The airplane (The New Piper Aircraft) representative reported that "examination of the engine, airframe, and fuel system found no indication of mechanical deficiency. However, significant amounts of material contamination, corrosion and rust were found in the low areas of the fuel system indicating that water had been present at some time and was allowed to remain in the system." He added that "it is necessary for the pilot to select each tank with the fuel selector valve then individually drain it, from the cockpit, prior to flight, using the drain valve on the fuel selector. The individual tanks are not equipped with drain sumps." He further stated that "if a fuel tank, that was not drained properly, were switched on during flight, water and/or contaminants may be introduced into the engine causing a partial loss of power or engine stoppage."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW00LA081