N48821

Substantial
None

Cessna 152 S/N: 15280983

Accident Details

Date
Wednesday, March 1, 2000
NTSB Number
FTW00LA089
Location
FORT WORTH, TX
Event ID
20001212X20494
Coordinates
32.979949, -97.309043
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot's failure to maintain aircraft control during landing. A factor was the crosswind condition.

Aircraft Information

Registration
N48821
Make
CESSNA
Serial Number
15280983
Engine Type
Reciprocating
Year Built
1977
Model / ICAO
152 C152
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
HODGE ANTHONY W
Address
309 MARSEILLEI
Status
Deregistered
City
HURST
State / Zip Code
TX 76054
Country
United States

Analysis

On February 29, 2000, at 1825 central standard time, a Cessna 152, single-engine airplane, N48821, struck a railroad track and terrain during an aborted landing near Fort Worth, Texas. The airplane was owned and operated by Split S Aviation of Fort Worth, Texas, as a 14 Code of Federal Regulations Part 91 solo instructional flight. The student pilot, sole occupant, was not injured, and the airplane sustained substantial damage. Visual meteorological conditions prevailed for the local flight, and a flight plan was not filed. The flight originated from Hicks Airfield Airport, Fort Worth, Texas, for a series of touch and go landings.

The pilot reported that, during the turn from a right base to final approach for runway 32, he overshot the runway and corrected the ground track back to the left. During the landing/flare touchdown, the airplane touched down on the right main landing gear, bounced to the left main landing gear, and turned 45 degrees to the runway. The pilot added full power, and the aircraft started to climb; however, the left wing struck a tree. Subsequently, the airplane spun around, the left wing hit a railroad track, and the nose landing gear dug into the terrain. The airplane slid down the railroad track before jumping off the track and coming to rest 60 feet west of the runway centerline. Winds were from 300 degrees at 6 knots.

The FAA inspector, who responded to the site, found the engine mounts and firewall damaged. The left wing was buckled with the upper cabin area wrinkled and buckled. The aft fuselage was split and buckled. The nose landing gear and engine cowling were damaged.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW00LA089