N1556H

Destroyed
Fatal

Cessna 177RG S/N: 177RG0730

Accident Details

Date
Wednesday, March 22, 2000
NTSB Number
MIA00FA117
Location
COLUMBIA, SC
Event ID
20001212X20688
Coordinates
33.990592, -81.000137
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The PIC's inadequate planning and preparation resulting in refueling not being performed and the subsequent fuel exhaustion and forced landing into trees. A factor in the accident was the erratic operation of the right fuel tank quantity indicating system.

Aircraft Information

Registration
N1556H
Make
CESSNA
Serial Number
177RG0730
Engine Type
Reciprocating
Year Built
1975
Model / ICAO
177RG C77R
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
AIRCRAFT HOLDING CO LLC
Address
3045 BEECHAVEN RD
Status
Deregistered
City
COLUMBIA
State / Zip Code
SC 29204-2752
Country
United States

Analysis

HISTORY OF FLIGHT

On March 22, 2000, about 1820 eastern standard time, a Cessna 177RG, N1556H, registered to Aircraft Holding Co., LLC, operating as a Title 14 CFR Part 91 personal flight, crashed during an emergency landing at Columbia, South Carolina. Visual meteorological conditions prevailed and no flight plan was filed. The airplane was destroyed, the private-rated pilot was seriously injured, and a private pilot-rated passenger was fatally injured. The flight originated from the same airport about 10 minutes before the accident.

According to another pilot who was in the landing pattern at Columbia Owens Downtown Airport when N1556H announced on unicom frequency that he was taxiing onto runway 31 for takeoff, intending to stay in the pattern, the departure and crosswind turn appeared normal. The other pilot completed a touch-and-go landing and lost sight of N1556H somewhere during his, (N1556's) downwind leg. The other pilot heard N1556H begin his "on base" call, pause for a few seconds, and then transmit that he was declaring an emergency because of an engine failure, and that he didn't think he could make the field. At about 1850, the other pilot could see that rescue workers were on the scene.

PERSONNEL INFORMATION

The PIC/owner possessed a private pilot's license with single engine-land and instrument/airplane ratings. The PIC's logbook indicates he had logged 24.7 hours of PIC time in the airplane, and had accumulated a total of 449 flying hours. According to the PIC, although the pilot/passenger held a current private pilot's license, he had not flown, nor was he flying N1556H, at the time of the accident.

Two FAA inspectors interviewed the PIC/owner at the Richland Hospital, Columbia, South Carolina, on April 28, 2000. Any details pertinent to the day of the accident could not be recalled by the PIC. The PIC's submission of NTSB form 6120.1/2 on August 7, 2000, omitted any narrative of the accident. The FAA report of the hospital interview is an attachment to this report.

AIRCRAFT INFORMATION

The airplane had been purchased by the PIC/owner from a private owner and delivered from Caldwell, New Jersey, on December 30, 1999. At the time of the airplane's annual inspection on September 1, 1994, the accumulated tachometer time was 1576.5 hours, and at the time of it's annual on September 9, 1999, tachometer time was 1598.7 hours. The repair station work order associated with the 1999 annual inspection contained the following entries, (1) "Check fuel screen on servo found debris, flushed out with boost pump. Pull and check injectors, flow fuel thru fuel lines to injectors. OK. 2650 (rpm) reached at static run up awaiting pilot report." (2) "Remove gascolator and disassemble. Replace bad plunger valve and shaft o-ring. Reassemble and check for leaks, OK."

According to maintenance records, the left fuel quantity/oil pressure combination gage was replaced in September, 1995, in accordance with Cessna service kit, SK177-55, 58, and 52.

METEOROLOGICAL INFORMATION

Visual meteorological conditions prevailed at the time of the accident. For additional information, see Weather Information on page 4 of this report.

WRECKAGE AND IMPACT INFORMATION

Ground collision occurred about 1/2 mile from the threshold of runway 31, very near runway extended centerline in an area of trees and dense scrub underbrush running along the northern edge of railroad tracks. The airplane's left wingtip first impacted a 70-foot-tall pine tree located about 30 feet north of the northern edge of that railroad bed. Fragments of the fiberglass wingtip remained in the tree. The power supply for the left wingtip strobe light was found on the railroad bed abeam of the tree strike. A distance of about 160 feet further, on a heading of about 310 degrees, the main wreckage was located in the underbrush. The airplane came to rest inverted, intact but heavily battered, about 30 degrees nose down, heading about 320 degrees. The right cabin door had been removed by emergency personnel. About 18 inches aft of the wing trailing edge, the fuselage was bent downward until the vertical stabilizer contacted the ground. The wing fuel tanks had ruptured and both wing leading edges had been crushed flat corresponding to the angle of terrain impact. Fire rescue workers arrived within 7 minutes of the crash prepared to foam the wreckage; however, they reported that the wreckage site or surrounding area lacked any evidence of fuel spill. There was no odor of spilled fuel when they arrived, nor did they observe any leakage from the wings or engine.

The fuel caps and filler ports revealed a proper fit and there were no fuel stains present. There was no evidence of fuel spewage in the foliage and no residual fuel was found in either tank. The wing skin revealed no evidence of hydraulic bulging in the vicinity of the fuel tanks. The right tank's inner walls were dry and the left tank's inner walls revealed only beads of water. The landing gear were in the extended position and the flaps were retracted. The spinner revealed heavy non-rotational crushing. Both propeller blades were contained in the hub and revealed aft bending with little leading edge or rotational damage.

Aileron control continuity was confirmed from the flight controls to the cockpit yoke. Rudder, stabilator, and trim tab control continuity was confirmed from the flight surface to the firewall bulkhead. The stabilator trim was at about 5 degrees tab down. Both pilot's yokes had broken off their push/pull tubes. The lap belts and left side harness had been cut by emergency personnel. The right side harness was intact and found disconnected at the site. The lower attachment stud plastic bushing was missing. The fuel tank selector was positioned to the right tank. The fuel quantity gages indicated 1/8 tank on the right and empty on the left. The lower fuselage mounted twin fuel reservoir tanks were found intact and undamaged. They were drained and contained 1.5 oz. in the right, and 0.5 oz. in the left, of uncontaminated 100LL aviation fuel. The mixture control was 1 5/16 inch out, the throttle was full in, and the prop control was at full increase. Found in the wreckage was a computer generated technical article titled, "Sacramento Sky Ranch RSA Fuel Injection Troubleshooting".

Fuel feed line continuity was confirmed from each fuel tank to the engine- driven fuel pump using compressed air. The electric auxiliary fuel pump was powered and operated normally. The fuel flow divider was missing the inspection seal on the cover screws safety wiring, and the washers under the cover screws appeared new and shiny. The spark plugs exhibited a light gray to whitish coloring, electrode gaps were proper, and wear was minimal. Six quarts of uncontaminated oil were contained in the crankcase. Engine rotation produced compression at all four cylinders, and valve, accessory drive, and gear train continuity was confirmed. Pumping action was observed for fuel and oil. Spark was observed from all magneto towers upon rotation. The magneto timing to valve/piston relationship appeared proper. The induction, exhaust, and alternate air systems revealed no obstructions, and the exhaust pipe interiors were white in color.

MEDICAL AND PATHOLOGICAL INFORMATION

Toxicological testing of specimens of the PIC was conducted by Richland Hospital, Columbia, South Carolina. The medical records are an attachment to this report.

Postmortem examination of the passenger was conducted by Dr. Frank E. Barron, III, Richland County Coroner. Cause of death was attributed to multiple trauma due to airplane crash. Toxicological tests of specimens from the passenger were conducted at the Federal Aviation Administration Research Laboratory, Oklahoma City, Oklahoma. No ethanol was detected. Pseudoephedrine was present in the blood and urine. Ephedrine was present in the blood and urine. Phenylpropanolamine was present in the urine. These substances are present in over-the-counter medications for asthma, hay fever, and cold/cough symptoms. The passenger's widow stated that the passenger suffered the standard allergies and used an inhaler.

TEST AND RESEARCH

At the time of the accident the engine had not been overhauled since new, (1975) and had accumulated about 1621 hours. Textron Lycoming Service Instruction No.SI 1009AN, dated November 4, 1998, specifies time between overhauls for the IO-360-A1B6D series engine as 2,000 hours or 12 years.

According to the PIC, the airplane was last fueled at Orangeburg Municipal Airport, Orangeburg, South Carolina, on March 19, 2000, by himself. The tanks were topped off, and the amount added was 37.5 gallons. The receipt for that transaction is an attachment to this report. He states he does not remember flying the airplane at any time between parking the aircraft at CUB after the 30 minute flight from Orangeburg following the March 19th top off and the accident flight, 3 days later.

According to the widow of the passenger/pilot in the right seat, the aircraft had been acquired by the PIC in January 2000. Immediately before the sale, it had been based in New Jersey and used very little because its owner lost his pilot privileges for medical reasons, (22 hours in the last 5 years). She further stated she was present and observed the fueling of N1556H at Orangeburg on March 19, 2000.

According to Columbia Owens Downtown Airport's (CUB) only fixed-base operator, Midlands Aviation, N1556H became a tie-down customer on January 6, 2000. Midland's records reveal that fuel or oil was never purchased, nor had any maintenance been performed on N1556H by their personnel. On March 3, 2000, the PIC/owner purchased five Lycoming engine intake gaskets and four intake tube o-rings from Midlands parts department.

The fuel tank quantity sender units, as well as the cockpit mounted quantity gages were removed and sent to the Cessna factory for operational analysis, with FAA oversight. Th...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA00FA117