N75CM

Substantial
None

Mckinnis STEEN SKYBOLT S/N: 1

Accident Details

Date
Monday, March 20, 2000
NTSB Number
MIA00LA114
Location
TUSCALOOSA, AL
Event ID
20001212X20699
Coordinates
33.170162, -87.620857
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

a loss of engine power during climb due to fuel starvation which was caused by a fuel leak in the gascolator as a result of improper maintenance by the operator that resulted in the pilot making a forced landing during which the airplane sustained substantial damage.

Aircraft Information

Registration
Make
MCKINNIS
Serial Number
1
Engine Type
Reciprocating
Year Built
1975
Model / ICAO
STEEN SKYBOLT SA02
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
STEEN SKYBOLT

Registered Owner (Current)

Name
LOWE KENNETH W
Address
PO BOX 30416
City
SEA ISLAND
State / Zip Code
GA 31561-0416
Country
United States

Analysis

On March 20, 2000, about 1545 central standard time, a McKinnis Steen Skybolt, N75CM, registered to Alamo Aerobatics, and operated as a Title 14 CFR Part 91 business flight crashed on departure from Tuscaloosa Municipal Airport, Tuscaloosa, Alabama. Visual meteorological conditions prevailed and no flight plan was filed. The airplane received substantial damage, and the commercial-rated pilot and one passenger were not injured. The flight was originating at the time of the accident.

The pilot stated that he was flying the airplane to sell it for the owner/operator, and he had landed at Tuscaloosa to refuel. After departing Tuscaloosa, about 4 miles east of the airport, at an altitude of 1,500 feet, the engine ceased operating without any warning. The pilot said that he then executed an emergency landing in a municipal construction landfill, during which he hit a berm, and the airplane incurred substantial damage. The pilot who is also a certificated aircraft mechanic, with an inspection authorization, further stated that he examined the wreckage the following day with an FAA inspector and they determined that the cause of the engine stoppage was due to a massive fuel leak at the gascolator. The gascolator thumb nut had not been safety wired, and it had backed off, allowing fuel to pour out the top of the gascolator unit. The airplane had accumulated 10 hours since its last condition inspection, which according to the pilot, had been performed by the owner/operator.

According to the FAA inspector, after tightening the bolt and applying fuel boost pressure to the fuel strainer, no fuel leaks were noted. The inspector further stated that the fuel in the airplane's fuel tank, as well as the fuel in the truck at the last refueling stop were both examined, and no fuel contamination was found.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA00LA114