N2RM

Destroyed
Fatal

Beech F33A S/N: CE-567

Accident Details

Date
Friday, May 26, 2000
NTSB Number
LAX00FA206
Location
COLUMBIA, CA
Event ID
20001212X21026
Coordinates
38.109127, -120.380653
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
2
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The pilot's failure to abort the downwind takeoff and his failure to attain flying speed.

Aircraft Information

Registration
N2RM
Make
BEECH
Serial Number
CE-567
Engine Type
Reciprocating
Model / ICAO
F33A BE33
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
MEYERHOFF RICHARD DAVID
Address
181 28TH AVE
Status
Deregistered
City
SAN FRANCISCO
State / Zip Code
CA 94121-1052
Country
United States

Analysis

HISTORY OF FLIGHT

On May 26, 2000, about 1630 hours Pacific daylight time, a Beech F33A, N2RM, was destroyed during the takeoff/initial climb from Columbia, California. The commercial rated pilot and non-rated passenger both received fatal injuries. Visual meteorological conditions prevailed for the personal flight operating under 14 CFR Part 91. No flight plan was filed. The originating flight was destined for Oakland, California, the airplane's base. The purpose for the landing at Columbia is unknown. Prior to landing at Columbia, the airplane had departed North Las Vegas, Nevada, at 1154, on a VFR flight plan destined for Columbia, by way of Beatty, Bishop, and Mammoth.

The Safety Board investigator talked by phone to witnesses that watched the airplane depart on runway 17. It became airborne about midfield and flew nose high 10/20 feet above the runway. Engine power was reduced, then reapplied, and the airplane crossed the runway end about 20 feet above ground level with the landing gear extended. One witness was sitting in an airplane doing an after maintenance run-up as he watched the accident airplane. The airplane collided with trees about 1,300 feet beyond the runway end. A postaccident fire erupted upon impact. One pilot witness reported the wind to be 290 degrees at 14 knots with a density altitude of 3,900 feet. Five telephonic witness interviews obtained by a Federal Aviation Administration (FAA) inspector are also attached to this report.

PERSONNEL INFORMATION

The pilot's logbook was recovered from the wreckage. The logbook documented a commercial check ride for the issuance of the commercial rating on June 16, 1999, in a Cessna 172RG. It also documented the last flight for 1999 as August 28, 1999, in the accident airplane. The next documented flight was May 19, 2000, as a local flight with a route from Oakland to Grants Pass and Eugene, Oregon. The last page indicated a total flight time of 1,308.9 hours.

AIRCRAFT INFORMATION

Airplane and engine logbook copies were obtained from the insurance company representative. According to the logbooks, the last recorded annual inspection occurred on June 14, 1999, at 2,763 total flight hours.

The engine was shipped to Continental Motors in Mobile, Alabama, for examination under the supervision of an FAA inspector from the Atlanta, Georgia, MIDO/MISO. According to the report, "this engine exhibits normal operational signatures throughout, except for the extensive fire and impact damages. All internal components appeared well lubricated. This engine did not exhibit any condition that would have caused an operational problem." The Continental report is attached.

WRECKAGE AND IMPACT INFORMATION

The wreckage was located approximately 1,300 feet off the departure end of runway 17. In the vicinity of the wreckage damaged trees were noted. A postcrash fire consumed major portions of the airframe and all of the center section.

The propeller was buried in the ground with only the spinner back plate flange, severed engine flange, and parts of two of the three propeller blades visible. Examination of the propeller blades revealed one with a severed blade tip measuring about 8 inches, with the blade bent aft, and one blade with slight forward bending at the outboard 7 or 8 inches. The third blade had slight damage. Two of the three damaged blades were loose from their respective pitch change blocks.

MEDICAL AND PATHOLOGICAL INFORMATION

On May 29, 2000, the Tuolumne County Medical Examiner performed an autopsy on the pilot. During the procedure, the FAA Civil Aeromedical Examiner in Oklahoma City, Oklahoma, obtained samples for toxicological analysis. The results of the analysis were negative for carbon monoxide, volatiles, and drugs. Cyanide was detected in the blood sample at a level of 0.72 (ug/ml).

ADDITIONAL INFORMATION

On June 13, 2001, the wreckage was released to the insurance company representative.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX00FA206