N66206

Substantial
None

Waco AGC-8 S/N: 5073

Accident Details

Date
Wednesday, August 16, 2000
NTSB Number
DEN00LA154
Location
OGDEN, UT
Event ID
20001212X21712
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

The pilot's failure to maintain directional control of the aircraft during landing roll. Factors were a tail wind, inadequate weather evaluation by the pilot, and lack of experience in make and model.

Aircraft Information

Registration
Make
WACO
Serial Number
5073
Engine Type
Reciprocating
Model / ICAO
AGC-8 WACC
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
5
FAA Model
AGC-8

Registered Owner (Current)

Name
VENALECK JOHN T SR
Address
7621 KENNETH DR
City
CONCORD TOWNSHIP
State / Zip Code
OH 44077-8992
Country
United States

Analysis

On August 16, 2000, at 1424 mountain daylight time, a Waco AGC-8, N66206, went off the left side of the runway, sheared the right main landing gear, damaged both right wings, and went nose down during landing roll at Ogden Hinckley Field, Ogden, Utah. The aircraft sustained substantial damage and the private pilot and his two passengers were not injured. Visual meteorological conditions prevailed for this cross-country flight from Klamath Falls, Oregon, operating under Title 14 CFR Part 91, and no flight plan was filed.

At the time of the accident, the wind was a left quartering tailwind at 6 knots.

According to the pilot, a "slight" bounce occurred during initial touchdown and the aircraft drifted left of the runway centerline. The pilot said he applied full right rudder followed by full right brake. Neither corrected the left drift, and the aircraft departed the left side of the runway into soft terrain.

According to witnesses, the aircraft bounced divergently several times during the touchdown phase of the landing and then veered off the left side of the runway and came to rest left wing down and nose down.

Inspection of the aircraft by an FAA airworthiness inspector provided no evidence of mechanical failure or malfunction.

Examination of the pilot's flight experience revealed the pilot had 7 hours in make and model, all of which was in the preceding 30 days.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DEN00LA154