N345JM

Substantial
None

Morrison E-RACER S/N: 113

Accident Details

Date
Tuesday, September 12, 2000
NTSB Number
CHI00LA298
Location
SUGAR GROVE, IL
Event ID
20001212X21931
Coordinates
41.759449, -88.449295
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

the owner/builder's inadequate modification to the engine air intake system and the inadvertent engine shutdown. Factors included the low air pressure of the air intake system and the excessive fuel flow to the manifold.

Aircraft Information

Registration
N345JM
Make
MORRISON
Serial Number
113
Engine Type
Reciprocating
Year Built
0000
Model / ICAO
E-RACER BPAT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
MORRISON JOHN K
Address
625 BLACKBERRY RIDGE DR
Status
Deregistered
City
AURORA
State / Zip Code
IL 60506-8993
Country
United States

Analysis

On September 12, 2000, at 1730 central daylight time, an experimental Morrison E-Racer, N345JM, was substantially damaged when it landed in a bean field near Sugar Grove, Illinois, after it had experienced a loss of power. The private pilot was not injured. The 14 CFR Part 91 flight had departed from Aurora Municipal Airport (ARR), Aurora, Illinois, at 1655 on a local test flight. The airplane was on a left base to runway 33 when it experienced a loss of power. An emergency landing was made to a bean field about 1/2 mile south of the airport. Visual meteorological conditions prevailed and no flight plan was filed.

The pilot reported he was performing a test flight to test the cylinder head cooling ducts. On the left base to final approach to runway 33 at ARR, the airplane had a total loss of power. The pilot reported, "... because of altitude and time, a emergency landing was made to a bean field 1/2 to 1/4 mile from RW 33." The pilot reported he had extended the turn to base due to traffic in the landing pattern.

The pilot reported that he had modified the airplane with a relief pressure valve in the air intake so that supercharged air could be vented prior to the fuel servo when the engine was at idle. The pilot reported that on the accident flight the engine was flooded with fuel when the throttle was pulled back to idle. The engine quit and a forced landing was executed.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI00LA298