N4914J

Substantial
None

Piper PA-28R-180 S/N: 28R-30633

Accident Details

Date
Monday, November 27, 2000
NTSB Number
ATL01LA014
Location
MERRITT ISLAND, FL
Event ID
20001218X45433
Coordinates
28.319526, -80.679183
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

Maintenance personnel failure to properly install engine cowling fasteners, which allowed the engine cowling to separate in flight.

Aircraft Information

Registration
N4914J
Make
PIPER
Serial Number
28R-30633
Engine Type
Reciprocating
Year Built
1968
Model / ICAO
PA-28R-180 P28R
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
CAMPBELL SEAN F
Address
5300 LOVETT DR
Status
Deregistered
City
MERRITT ISLAND
State / Zip Code
FL 32953-7341
Country
United States

Analysis

On November 27, 2000, at 1730 eastern standard time, a Piper PA-28R-180, N4914J, had its engine cowling separate from the airplane during takeoff climb from Merritt Island Airport, Merritt Island, Florida. The airplane was operated by the commercial pilot under the provisions of Title 14 CFR Part 91 and visual flight rules. Visual meteorological conditions prevailed and no flight plan was filed for the local flight. The pilot was not injured and the airplane sustained substantial damage. The flight was originating from Merritt Island, Florida, at the time of the accident.

According to the pilot, this was his second flight of the day. He taxied to runway 29 and departed to the west. He said he noted nothing out of the ordinary on takeoff or climb out until reaching about 500 feet when the engine cowling separated from the airplane. From where he sat he believed the front left side separated first, shook violently then rolled toward the right rear side. The cowling broke off a piece of the right windscreen, spun off and hit the baggage door and finally collided with the stabilator. The pilot stated that he made a gentle left turn to downwind and landed the airplane safely on runway 29. He recalled seeing nothing to indicate a loose cowling during his preflight inspection.

Examination of the engine cowling found impact damage around the nose/intake area, and was also cracked just forward of the oil access door. The forward reinforced composite structure had separated from the cowling and was broken into four pieces. This structure contained the cowl alignment pins, and there was no abnormal wear observed between the cowl pins, or the pin receptacles located on the lower cowling. Examination of the upper cowling revealed that three of the four fastener assembly studs were missing. The remaining stud was located on the left, rear fastener assembly, and was held in place by a retainer ring. Closer examination of the left-rear cowl latch fastener assembly revealed during the operational test that the stud positively engaged the receptacle when turned 1/4 turn clockwise. Some looseness remained between the fastener and the associated receptacle. The tip of the stud had a polished appearance, but did not appear to be excessively worn. Review of the airplane maintenance logs revealed that the brake hydraulic system was serviced on November 17, 2000, about 7 flight hours before the mishap.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ATL01LA014