N3143A

Substantial
None

Cessna 170BS/N: 25787

Accident Details

Date
Tuesday, May 8, 2001
NTSB Number
ANC01LA055
Location
FAIRBANKS, AK
Event ID
20010510X00924
Coordinates
64.813613, -147.859725
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

A failure of the tailwheel spring assembly due to fatigue during touch and go landings. A factor in the accident was an inadequate annual inspection by maintenance personnel.

Aircraft Information

Registration
Make
CESSNA
Serial Number
25787
Engine Type
Reciprocating
Year Built
1953
Model / ICAO
170BC170
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
170B

Registered Owner (Current)

Name
SKYLINE HOLDINGS LLC
Address
PO BOX 520776
City
BIG LAKE
State / Zip Code
AK 99652-0776
Country
United States

Analysis

On May 7, 2001, at 1956 Alaska daylight time, a wheel-equipped Cessna 170B airplane, N3143A, sustained substantial damage during landing at the Fairbanks International Airport, Fairbanks, Alaska. The airplane was being operated as a visual flight rules (VFR) local area instructional flight when the accident occurred. The airplane was operated by the student pilot/owner. The commercial certificated pilot/flight instructor, and the student pilot, were not injured. Visual meteorological conditions prevailed. The flight originated at the Fairbanks International Airport at 1917.

During a telephone conversation with the National Transportation Safety Board (NTSB) investigator-in-charge (IIC), on May 9, 2001, the flight instructor reported that he was seated in the right seat, and was conducting wheel landings with the student on the ski strip, runway 19, at Fairbanks. During the touchdown on the third or fourth landing, the tailwheel assembly suddenly broke off.

A Federal Aviation Administration (FAA) airworthiness inspector, Fairbanks Flight Standards District Office (FSDO), examined the airplane after the accident. He reported he found a preexisting crack in the tailwheel spring assembly that was about 1/16 inch deep, and about 1/2 inch long. He said the spring failed at the crack, and when the tailwheel departed the airplane, it struck the bottom of the rudder, and the rudder trim tab. The bottom and aft portion of the rudder assembly was torn open.

In the Pilot/Operator Report (NTSB form 6120.1/2) submitted by the student pilot/owner, the owner indicated the tailwheel spring had a total time of 162 hours. The 6120.1/2 report noted an annual inspection was conducted on November 6, 2000, 65 hours before the accident.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ANC01LA055