N6647M

Substantial
Serious

Stinson 108-3S/N: 108-4647

Accident Details

Date
Thursday, July 5, 2001
NTSB Number
NYC01LA164
Location
Friendly, MD
Event ID
20010712X01390
Coordinates
38.729728, -77.000595
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
1
Uninjured
0
Total Aboard
2

Probable Cause and Findings

A baffling failure within the exhaust system. Factors were an inadequate annual inspection and the pilot's operation of the airplane with known deficiencies in equipment.

Aircraft Information

Registration
N6647M
Make
STINSON
Serial Number
108-4647
Engine Type
Reciprocating
Year Built
1948
Model / ICAO
108-3S108
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
WILLIAMS ALAN L
Address
1816 ROCKING HORSE DR
Status
Deregistered
City
SIMI VALLEY
State / Zip Code
CA 93065-5912
Country
United States

Analysis

On July 5, 2001, about 1100 eastern daylight time, a Stinson 108-3, N6647M, was substantially damaged during a forced landing, after takeoff from Potomac Airfield (VKX), Friendly, Maryland. The certificated private pilot sustained minor injuries, and the passenger was seriously injured. Visual meteorological conditions prevailed, and no flight plan was filed for the personal conducted under 14 CFR Part 91.

The pilot reported that he purchased fuel at VKX, and intended to return to his home airport, Washington Executive Airport (W32), Clinton, Maryland, located about 2 miles to the east. The pilot added that he started the engine, taxied to runway 24, and performed a magneto check. No anomalies were observed, and the pilot initiated a takeoff roll. However, the engine began to run rough, and the pilot aborted the takeoff. He then ran the engine at different RPM, and performed a second satisfactory magneto check. During the second takeoff roll, the engine ran rough again, and the pilot aborted the takeoff. The pilot then let the engine run for 5 minutes at different RPM, and it passed a third magneto check. On the third takeoff attempt, the engine "had good power," but as the airplane climbed above the trees, the engine lost all power. The pilot performed a forced landing into trees, and the airplane settled to the ground in a wooded area.

A Safety Board investigator and Federal Aviation Administration (FAA) inspector examined the engine after the wreckage was recovered. They observed that the right-side muffler baffling was mostly disintegrated, consistent with a baffling failure and subsequent blockage of the engine exhaust. The FAA inspector stated that the muffler was manufactured by Hanlon Wilson Muffler Systems, and the baffling was required to be inspected for cracks and wear during the annual inspection of the airplane.

The last annual inspection of the airplane was performed on March 22, 2001, and the airplane had accumulated approximately 28 hours of operation since that inspection.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC01LA164