N63262

Destroyed
Fatal

Cessna 150MS/N: 15077213

Accident Details

Date
Monday, November 12, 2001
NTSB Number
CHI02FA025
Location
Dyer, IN
Event ID
20011203X02330
Coordinates
41.410556, -87.517219
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
2
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The failure of the flight crew to maintain adequate airspeed, resulting in an inadvertent stall/spin and the flight instructor's inadequate supervision of the flight, his impairment due to the use of over-the-counter medication is a contributing factor.

Aircraft Information

Registration
N63262
Make
CESSNA
Serial Number
15077213
Engine Type
Reciprocating
Year Built
1975
Model / ICAO
150MC150
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
NEMET PETER
Address
11300 S EWING AVE
Status
Deregistered
City
CHICAGO
State / Zip Code
IL 60617-7019
Country
United States

Analysis

HISTORY OF FLIGHT

On November 12, 2001, at 1550 central standard time, a Cessna 150M, N63262, operated by Chicago Business Air Center, Lansing, Illinois, was destroyed during an in-flight collision with the terrain following a loss of control while maneuvering near Dyer, Indiana. Visual meteorological conditions prevailed at the time of the accident. The instructional flight was operating under the provisions of 14 Code of Federal Regulations (CFR) Part 91 without a flight plan. The certified flight instructor (CFI) and his dual student were fatally injured. The local flight departed the Lansing Municipal Airport (IGQ), Lansing, Illinois, at 1538.

Aircraft radar track data was obtained from Federal Aviation Administration (FAA) Air Traffic Control. The data indicated there was a single aircraft transmitting a visual flight rules (VFR) 1200 transponder beacon code near the accident location around the time of the accident. The aircraft radar track data was plotted on a sectional chart, and the track traced back to the departure airport.

According to the radar data, the first radar return for the accident aircraft was recorded at 1538:40.94 [Time Format = hhmm:ss.ss]. The aircraft departed the IGQ runway 09 traffic pattern to the south and climbed to a pressure altitude that varied between 2,600 and 2,700 feet. At 1547:18.05, the aircraft initiated a left turn toward the east followed by a right turn back to toward the south at 1547:59.52. The aircraft continued on a southern course at a pressure altitude between 2,600 and 2,700 feet until 1549:50.39, when the aircraft changed to a northern course. The last 1200 beacon code radar return was recorded at 1549:59.55 at a pressure altitude of 2,100 feet. At 1550:17.90, the radar data began tracking a series of 7700 transponder beacon code radar returns. The last 7700 beacon code radar return was recorded at 1550:41.21 at a pressure altitude of 900 feet.

The last minute of radar track data was recorded as follows:

Time; Transponder Code; Latitude (North); Longitude (West); Pressure Altitude (Feet)

1549:41.15; 1200; 41.402540; 87.514554; 2700

1549:45.69; 1200; 41.402163; 87.514117; 2700

1549:50.39; 1200; 41.401366; 87.513983; 2700

1549:55.01; 1200; 41.402814; 87.514085; 2200

1549:59.55; 1200; 41.404776; 87.514801; 2100

1550:17.90; 7700; 41.409681; 87.515118; 1700

1550:22.74; 7700; 41.411007; 87.515145; 1600

1550:27.25; 7700; 41.411698; 87.516755; 1300

1550:31.76; 7700; 41.410786; 87.518764; 1200

1550:36.59; 7700; 41.409586; 87.518890; 1200

1550:41.21; 7700; 41.409787; 87.517581; 0900

A plot of the aircraft radar track data, along with the source data, is included with the docket material associated with this factual report.

A witness to the accident was driving north on Calumet Avenue, near the intersection of Calumet Avenue and 113th Avenue, when she witnessed an airplane "flying very low & at first glance it looked to be upside down." The witness stated that she turned to tell her child about the airplane, and when she directed her attention back to the airplane she only saw a cloud of dirt and dust rising from the cornfield. The witness reported there was "no fire, smoke, or explosion" when the airplane impacted the field. The witness stated she thought the airplane had made a "rough landing" and did not report being a witness until the day after the accident.

Another witness was working on his residence, between 1545 and 1600, when he saw an "airplane, nose-down, falling like a rock." The witness reported the airplane was "small" and at the time he thought it was a "model airplane." He reported being a witness to the accident at a later date. The witness stated the airplane was descending rapidly, unlike a normal landing approach. The witness reported that he did not hear the airplane impact the terrain or see any smoke.

A written witness statement and several memorandums of conversation are included with the docket material associated with this factual report.

The Civil Air Patrol detected an emergency locator transmitter signal and subsequently, with the assistance of local law enforcement, located the wreckage on November 13, 2001, at 0010 local time.

PERSONNEL INFORMATION

Pilot-In-Command (PIC):

The CFI was the PIC and was seated in the right cockpit position. He held a commercial pilot certificate with airplane single-engine land, airplane multiengine land, and instrument airplane ratings. The FAA issued the commercial pilot certificate on November 21, 1998. He also held a CFI certificate with airplane single-engine land and instrument airplane ratings. The most recent CFI certificate was issued on July 7, 2000.

FAA records indicate his last medical examination was completed on March 22, 2001, and that he was issued a second-class medical certificate with no restrictions or limitations.

According to the pilot's flight logbook, he had accumulated a total flight time of 1,447.4 hours, of which 1,267.0 hours were as PIC. He had accumulated 1,339.0 hours in single-engine airplanes, 105.4 hours in multiengine airplanes, and 3.1 in helicopters. Since the issuance of his initial flight instructor certificate on May 15, 2000, he had given 964.2 hours of dual instruction. He had logged 4.9 hours in the Cessna 150, all of which were as CFI. He flew 115.4 hours during the previous 3 months, including 4.0 hours in the accident airplane. He had flown 45.0 hours during the prior 30 days, of which 2.7 hours were in the accident airplane. He flew 3.9 hours during the last 24 hours, including 0.7 hours in the accident airplane.

The pilot's last flight review, as required by 14 CFR Part 61.56, was satisfied on July 7, 2000, after the successful completion of his instrument flight instructor checkride.

For the period between September 18, 1996, and November 12, 2001, the pilot logged one flight that included spin entries, spins, and spin recoveries. The flight was completed on March 18, 2000, and was flown to satisfy FAR 61.183(i), which is a requirement for the initial certified flight instructor certificate. The spin flight consisted of eight spins and was completed in a Cessna 172.

Selections from the CFI's flight logbook are included with the docket material associated with this factual report.

Dual Student:

The dual student was receiving flight instruction and was seated in the left cockpit position. The dual student did not hold any pilot certificates and had not applied for a student pilot certificate, according to FAA records. The dual student did not possess a medical certificate.

According to the dual student's flight logbook, his first recorded flight was on August 11, 2001. He received all of his flight instruction from the above-mentioned CFI. The dual student had accumulated a total flight time of 4.6 hours, all of which were dual instruction given in the accident airplane. He flew 4.0 hours during the previous 3 months, 2.7 hours during the last 30 days, and 0.7 hours during the last 24 hours.

The dual student had logged flight instruction for the following maneuvers: turns, climbs, descents, slow flight, power-off stalls, power-on stalls, and steep turns.

Selections from the dual student's flight logbook are included with the docket material associated with this factual report.

AIRCRAFT INFORMATION

The accident airplane was a Cessna 150M, serial number 15077213. The Cessna 150M is a single engine, high-wing airplane. The Cessna 150M is equipped with a fixed tricycle landing gear, electrically actuated wing flaps, and is powered by a single reciprocating engine. The fuselage and empennage are of an all-metal semimonocoque design. The wings are externally braced and have two metal fuel tanks. The airplane was equipped with dual controls and two cockpit seats. The accident airplane had a certified maximum takeoff weight of 1,600 lbs and a maximum useful load of 483.1 lbs.

The airplane was issued a Standard Airworthiness Certificate on August 27, 1975, and was certified as a utility category airplane. The accident airplane had accumulated a total flight time of 4,156.8 hours since new.

The last annual inspection was completed on February 9, 2001, and the airplane had accumulated 151.3 hours since the inspection. The last airframe inspection, a 100-hour inspection, was performed on August 13, 2001, at 4,104.7 hours total time. The airplane had accumulated 52.1 hours since the last inspection. According to the aircraft maintenance logbooks, all applicable FAA Airworthiness Directives had been complied with as of the last inspection.

The engine was a 100 horsepower Teledyne Continental Motors O-200-A48, serial number 275772-R. The engine had accumulated 848.8 hours since the last factory overhaul, which was completed on September 29, 1987. The engine was installed on the accident airplane on October 8, 1987. The last engine inspection, a 100-hour inspection, was performed on August 13, 2001, and the engine had accumulated 52.1 hours since the last inspection.

The propeller was a two-bladed McCauley 1A102, serial number K20666.

The aircraft's Pilot Operating Handbook (POH) included a "Revised Weight and Balance Data" sheet, dated July 11, 1989, which listed the following information:

New Empty Weight 1,116.9 lbs

New Empty Weight CG 32.6 inches

New Useful Load 483.1 lbs

New Empty Weight Moment 36,392.0 in/lbs

The POH listed the Cessna 150M certificated maximum gross weight as 1,600 lbs.

The CFI's weight, as reported in the Lake County Autopsy Report, was 161 lbs.

The dual student's weight, as reported in the Lake County Autopsy Report, was 208 lbs.

According to company fueling records and personnel interviews, the airplane was fully fueled prior to the accident flight. The Cessna 150M POH lists the maximum usable fue...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI02FA025