N1016T

Destroyed
None

Beech 95S/N: TD-108

Accident Details

Date
Friday, December 14, 2001
NTSB Number
LAX02LA047
Location
Kingman, AZ
Event ID
20011219X02421
Coordinates
35.259445, -113.938056
Aircraft Damage
Destroyed
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

the pilot's failure to complete and verify the prelanding checklist and extend the landing gear, which resulted in the gear-up landing.

Aircraft Information

Registration
N1016T
Make
BEECH
Serial Number
TD-108
Engine Type
Reciprocating
Year Built
1958
Model / ICAO
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
SHEBLE AVIATION & FLIGHT SCHOOL INC
Address
600 HIGHWAY 95
Status
Deregistered
City
BULLHEAD CITY
State / Zip Code
AZ 86429-5007
Country
United States

Analysis

On December 13, 2001, at 1745 mountain standard time, a Beech 95, N1016T, was destroyed by fire following a gear-up landing at Kingman, Arizona. Neither the commercial pilot nor the pilot rated passenger were injured. The airplane was being operated by Sheble Aviation & Flight School, Inc., under the provisions of 14 CFR Part 91, as a positioning flight. Visual meteorological conditions prevailed, and a flight plan had not been filed for the cross-country flight that originated from Needles, California, at 1715.

The airplane had been flown to the Sheble maintenance provider, located in Needles, earlier in the day for a "slow to retract" landing gear problem. According to the maintenance technician, he replaced the retract motor and swung the landing gear several times to check the system, including the landing gear warning horns. A Sheble pilot and a prospective student pilot passenger picked up the airplane.

According to the pilot's written statement, he conducted a prelanding check and entered a 5-mile final for runway 03. He stated that he performed a "couple more" landing checks and told the student/passenger about the airspeeds to expect during the different phases of the landing. As the airplane crossed the runway threshold, the pilot pulled the power levers to idle and transitioned to the flare. The pilot noticed that the airplane started to "sink," and he couldn't believe that he had flared that high. He started to inform the passenger that it was going to be a hard landing when the airplane "slammed" down onto the runway.

The airplane skidded to a stop, and the pilot noticed flames down by his left leg. He started to tell the passenger to get out of the airplane only to hear the passenger state the same thing. As the pilot and passenger walked away from the airplane, the airplane became engulfed in flames.

The pilot stated that he could not remember whether he put the landing gear down or not, but he did mention not noticing any landing gear warning horns during the landing.

Post accident photographs of the airplane revealed that the entire cockpit and cabin area had been consumed by fire. Due to the fire damage the landing gear and warning systems could not be tested.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX02LA047