N1211D

Destroyed
Fatal

Cessna 170AS/N: 20112

Accident Details

Date
Friday, May 17, 2002
NTSB Number
DEN02FA043
Location
Casper, WY
Event ID
20020530X00783
Coordinates
42.985553, -106.748611
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

the pilot's inadvertent flight into adverse weather conditions and his subsequent failure to maintain aircraft control. A factor contributing to this accident was the fog.

Aircraft Information

Registration
Make
CESSNA
Serial Number
20112
Engine Type
Reciprocating
Year Built
2008
Model / ICAO
170AC170
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
LC41-550FG

Registered Owner (Current)

Name
WEST RIDGE TTX LLC
Address
6404 SOUTHRIDGE PKWY
City
PARKER
State / Zip Code
TX 75002-5534
Country
United States

Analysis

HISTORY OF FLIGHT

On May 17, 2002, approximately 0238 mountain daylight time, a Cessna 170A, N1211D, piloted by a non-instrument rated private pilot, was destroyed when it impacted terrain 15 nautical miles west-northwest of the Natrona County International Airport (CPR), Casper, Wyoming. Night visual meteorological conditions with observed dense fog prevailed at the time of the accident. The personal, cross-country flight was being conducted on a visual flight rules flight plan from CPR to Thermopolis, Wyoming, under the provisions of Title 14 CFR Part 91. The pilot sustained fatal injuries. The flight originated at 0228.

The pilot's wife said that the pilot took off from Watkins, Colorado, for Thermopolis, on May 16, 2002, about 1900. She said she told him that they were experiencing bad weather but it was moving rapidly to the east. The pilot's wife said she next spoke to the pilot about 2230. He told her that he was at Casper, Wyoming. He told her that he diverted around stormy weather and was going to wait until it cleared. The pilot's wife said he called her again at 0030 and told her the weather was still down and that he would be spending the night at Casper. He told her that he was going to stop at the Flight Service Station and see what they had to say. He told her that he would then sleep in the airplane until sunrise and not to expect him.

The pilot's wife said she received a call about 0400 from Flight Service asking if the pilot had gotten home and forgot to close his flight plan. She told them that he wasn't there , but would go up to the Thermopolis Airport to see if he was there. She said that Flight Service told her that the pilot waited at their office until 0230 when the weather began to clear up. He left after that.

At 0600, the pilot's wife said she spoke with Flight Service and informed them that there was no sign of her husband. Search and rescue was initiated. The airplane was located by Civil Air Patrol personnel and Natrona County Sheriff's deputies approximately 0730.

PERSONNEL INFORMATION

The pilot was an airframe and powerplant mechanic employed by a fixed base operator in Denver, Colorado. The pilot held a private pilot certificate with single engine and multi-engine land airplanes. The pilot's multi-engine land rating was restricted to centerline thrust.

According to the pilot's logbook, as of May 14, 2002, the pilot had 1,698.3 total flying hours, 1,642.3 hours in single engine land airplanes, and 1,572.7 hours as pilot-in-command. In the previous 30 days, the pilot logged 14.4 total flying hours, all of which was in N1211D. Of the 14.4 hours logged in the previous 30 days, 3.6 hours was at night.

The pilot successfully completed a flight review on May 21, 2001, in N1211D.

The pilot held a second class medical certificate dated November 5, 2001. The certificate showed the following limitation: "Holder shall wear corrective lenses.

AIRCRAFT INFORMATION

The airplane, serial number 20112, was manufactured in 1951. The airplane was owned and operated by the pilot and used for transportation to his job in Denver, Colorado, and for pleasure.

According to the airframe logbooks, the airplane underwent an annual inspection on January 1, 2002. The tachometer time recorded at the annual inspection was 2,541.5 hours. The tachometer time recorded at the accident scene was 2,587.7 hours.

The airplane was powered by a Continental O-300-A, carbureted engine rated at 145 horsepower at 2,700 rpm. The engine, serial number 6783-D-2-2, time since major overhaul was 1,627.3 hours.

METEOROLOGICAL INFORMATION

At 0203, the Aviation Routine Weather Report at CPR was scattered clouds at 1,100 feet, ceiling 2,000 feet overcast, visibility 10 statute miles, temperature 43 degrees Fahrenheit (F), dew point 39 degrees F, winds 360 degrees at 6 knots, and an altimeter setting of 30.20 inches of Mercury (Hg).

Civil Air Patrol personnel and Natrona County Sheriff's deputies, reported dense fog in the Casper area during the early morning hours.

WRECKAGE AND IMPACT INFORMATION

The NTSB on scene investigation began on May 17, 2002, at 1900.

The accident site was located in a pasture 2 miles south of U. S. Highway 20, and 15 miles west-northwest of the Natrona County International Airport. The site extended south along a 168-degree magnetic heading for approximately 373 feet.

The accident site began with a 29-foot long, 10-inch wide, and 3-inch deep scrape in the ground running along a 172-degree heading. At the beginning of the scrape were pieces of red glass; blue and white paint chips, and a wing tip light frame. Along the scrape were numerous paint chips, pieces of clear Plexiglas, and pieces from the airplane's left wing.

At the end of the scrape was an impact crater. The crater was 11 feet long, 6 feet wide, and 28 inches at its deepest point near the center. Within the crater were pieces of broken Plexiglas, white paint chips, and a crushed cabin air vent. The ground at the south edge of the crater was pushed upward. A spray of dirt extended outward from the south edge of the crater for approximately 23 feet. Within the spray of dirt were broken pieces from the airplane's cowling and right wing. Additionally, there were broken pieces of Plexiglas, paint chips, and parts from the engine exhaust manifold.

The airplane's propeller was located 62 feet from the initial ground contact point. The propeller was broken torsionally from the crankshaft just behind the flange. The propeller blades showed torsional bending, tip curling, and chordwise and diagonal-running scratches. There were several nicks in the leading edges of both blades.

A debris field, beginning at the propeller, extended south along a 168-degree heading for approximately 143 feet. The debris field was approximately 70 feet at its widest point. Within the debris field were the outboard portion of the right aileron, the left wing fuel tank, the left wing strut, left main landing gear strut, a part of the rudder pedal torque tube, pieces of the cabin's interior walls, pieces of cabin insulation, the right cabin door, several flight and engine instruments, pieces of broken clear Plexiglas, the right side upper cowling door, and numerous charts, manual pages, and personal effects.

A piece of the left doorframe was located 85 feet from the initial ground contact point. It was broken outward and crushed aft.

A piece of the instrument panel with the starter switch was located 90 feet from the initial ground contact point. The panel piece was broken and twisted. The switch was broken off.

The outboard section of the right aileron was located 123 feet from the initial ground contact point. It was broken off at the hinges, and was bent upward and twisted aft.

The left wing fuel tank was located 130 feet from the initial ground contact point. The tank was broken open, and bent and crushed inward. The smell of aviation fuel was prevalent on the ground south of the fuel tank. The upper right cowling door was located at 137 feet. It was broken longitudinally along the hinges and was bent outward.

A 9-foot, 6-inch section of the airplane's left wing forward spar, the left wing strut, and the left main landing gear strut, were located 162 feet from the initial ground contact point. The spar section was broken out, twisted, and bent aft. The left strut was intact and remained attached by the mounting bolts to the wing strut and a piece of the bottom fuselage and left main landing gear strut. The left main landing gear strut was intact. The wheel, brake, and brake line was broken off. The fuselage piece with the landing gear strut was broken out, crushed and twisted. The smell of aviation fuel was prevalent on the spar section and on the ground around the spar and strut.

A second impact scar was located at 179 feet from the initial ground contact point. The scar was approximately 2 feet long, 18 inches wide, and 8 inches at its deepest point. Just south of the hole were pieces of engine crankcase and a bent push rod. A spray of oil began 9 feet south of the second impact scar and ran along the ground on a 172 degree heading for 38 feet.

The right main cabin door was located 188 feet from the initial ground contact point. The door was broken at the hinges and crushed aft along the front edge of the door. The door window was broken out and fragmented.

The airplane's main wreckage was located 208 feet from the initial ground contact point. The wreckage consisted of the airplane's cabin, outboard portion of the left wing and aileron, the aft portion of the right wing, the right main landing gear, the aft fuselage, and the empennage.

Immediately before the main wreckage were broken pieces of the instrument panel, glareshield, several flight and engine instruments, and personal effects.

The airplane's forward cabin was broken open at the instrument panel and right front seat. The cabin front floor was broken open and crushed upward. The top of the front cabin was crushed downward and bent aft. The aft cabin floor was bent downward. The top of the aft cabin was buckled upward and crushed aft. The right aft cabin window was broken out and fragmented. The left aft cabin wall was broken open and crushed aft. The right main landing gear strut and wheel was broken forward and twisted at the front of the broken forward cabin section. The brake line was broken. The wheel and tire was intact.

The outboard section of the left wing and left aileron were crushed aft, bent upward, and twisted aft at mid-span. The left wing strut was intact and remained attached at the wing and fuselage mounting bolts. The left wing tip was broken aft longitudinally. The outboard wing at the wing tip rivet line was broken open and crushed aft. The bottom of the left inboard wing was crushed downward and bent aft. The left flap remained attached to the inboard wing s...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DEN02FA043